2b04495e21
Hulk Robot reports incorrect sp->rx_count_cooked value in decode_std_command(). This should be caused by the subtracting from sp->rx_count_cooked before. It seems that sp->rx_count_cooked value is changed to 0, which bypassed the previous judgment. The situation is shown below: (Thread 1) | (Thread 2) decode_std_command() | resync_tnc() ... | if (rest == 2) | sp->rx_count_cooked -= 2; | else if (rest == 3) | ... | sp->rx_count_cooked = 0; sp->rx_count_cooked -= 1; | for (i = 0; i < sp->rx_count_cooked; i++) // report error checksum += sp->cooked_buf[i]; sp->rx_count_cooked is a shared variable but is not protected by a lock. The same applies to sp->rx_count. This patch adds a lock to fix the bug. The fail log is shown below: ======================================================================= UBSAN: array-index-out-of-bounds in drivers/net/hamradio/6pack.c:925:31 index 400 is out of range for type 'unsigned char [400]' CPU: 3 PID: 7433 Comm: kworker/u10:1 Not tainted 5.18.0-rc5-00163-g4b97bac0756a #2 Hardware name: QEMU Standard PC (i440FX + PIIX, 1996), BIOS rel-1.14.0-0-g155821a1990b-prebuilt.qemu.org 04/01/2014 Workqueue: events_unbound flush_to_ldisc Call Trace: <TASK> dump_stack_lvl+0xcd/0x134 ubsan_epilogue+0xb/0x50 __ubsan_handle_out_of_bounds.cold+0x62/0x6c sixpack_receive_buf+0xfda/0x1330 tty_ldisc_receive_buf+0x13e/0x180 tty_port_default_receive_buf+0x6d/0xa0 flush_to_ldisc+0x213/0x3f0 process_one_work+0x98f/0x1620 worker_thread+0x665/0x1080 kthread+0x2e9/0x3a0 ret_from_fork+0x1f/0x30 ... Reported-by: Hulk Robot <hulkci@huawei.com> Signed-off-by: Xu Jia <xujia39@huawei.com> Signed-off-by: David S. Miller <davem@davemloft.net> |
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.. | ||
6pack.c | ||
Kconfig | ||
Makefile | ||
baycom_epp.c | ||
baycom_par.c | ||
baycom_ser_fdx.c | ||
baycom_ser_hdx.c | ||
bpqether.c | ||
hdlcdrv.c | ||
mkiss.c | ||
scc.c | ||
yam.c | ||
z8530.h |