Returning early from stm32_usart_serial_remove() results in a resource
leak as several cleanup functions are not called. The driver core ignores
the return value and there is no possibility to clean up later.
uart_remove_one_port() only returns non-zero if there is some
inconsistency (i.e. stm32_usart_driver.state[port->line].uart_port == NULL).
This should never happen, and even if it does it's a bad idea to exit
early in the remove callback without cleaning up.
This prepares changing the prototype of struct platform_driver::remove to
return void. See commit 5c5a7680e6 ("platform: Provide a remove callback
that returns no value") for further details about this quest.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Link: https://lore.kernel.org/r/20230512173810.131447-2-u.kleine-koenig@pengutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The stm32_usart_transmit_chars() may be called with empty or stopped
transmit queue, and no XON/OFF character pending. This can happen at
the end of transmission, where this last call is used to either handle
the XON/XOFF x_char, or disable TX interrupt if queue is empty or
stopped.
If that occurs, do not assert the RS485 RTS/DE GPIO anymore, as the
GPIO would remain asserted past the end of transmission and that would
block the RS485 bus after the transmission.
Only assert the RS485 RTS/DE GPIO if there is either pending XON/XOFF
x_char, or at least one character in running transmit queue.
Fixes: d7c7671616 ("serial: stm32: Use TC interrupt to deassert GPIO RTS in RS485 mode")
Signed-off-by: Marek Vasut <marex@denx.de>
Link: https://lore.kernel.org/r/20230223042252.95480-2-marex@denx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Requesting an interrupt with IRQF_ONESHOT will run the primary handler
in the hard-IRQ context even in the force-threaded mode. The
force-threaded mode is used by PREEMPT_RT in order to avoid acquiring
sleeping locks (spinlock_t) in hard-IRQ context. This combination
makes it impossible and leads to "sleeping while atomic" warnings.
Use one interrupt handler for both handlers (primary and secondary)
and drop the IRQF_ONESHOT flag which is not needed.
Fixes: e359b4411c ("serial: stm32: fix threaded interrupt handling")
Reviewed-by: Sebastian Andrzej Siewior <bigeasy@linutronix.de>
Tested-by: Valentin Caron <valentin.caron@foss.st.com> # V3
Signed-off-by: Marek Vasut <marex@denx.de>
Cc: stable@vger.kernel.org
Link: https://lore.kernel.org/r/20230120160332.57930-1-marex@denx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If a RX_DURING_TX GPIO is defined by the DT property "rs485-rx-during-tx-gpios"
this patch switches this GPIO accordingly to the RS485 flag RX_DURING_TX in user
space. Controlled by this GPIO, now the hardware is responsible for connecting
or disconnecting RX during TX.
Signed-off-by: Christoph Niedermaier <cniedermaier@dh-electronics.com>
Link: https://lore.kernel.org/r/20221202104127.122761-4-cniedermaier@dh-electronics.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If dma_request_chan() returns a PROBE_DEFER error, clk_disable_unprepare()
will be called and USART clock will be disabled. But early console can be
still active on the same USART.
While moving dma_request_chan() before clk_prepare_enable(), the clock
won't be taken in case of a DMA PROBE_DEFER error, and so it doesn't need
to be disabled. Then USART is still clocked for early console.
Fixes: a7770a4bfc ("serial: stm32: defer probe for dma devices")
Reported-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Link: https://lore.kernel.org/r/20221118170602.1057863-1-valentin.caron@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If CONFIG_SERIAL_EARLYCON and CONFIG_OF are both not set,
gcc warns about unused variable:
drivers/tty/serial/stm32-usart.c:83:32: error: ‘stm32h7_info’ defined but not used [-Werror=unused-variable]
static struct stm32_usart_info stm32h7_info = {
^~~~~~~~~~~~
drivers/tty/serial/stm32-usart.c:61:32: error: ‘stm32f7_info’ defined but not used [-Werror=unused-variable]
static struct stm32_usart_info stm32f7_info = {
^~~~~~~~~~~~
drivers/tty/serial/stm32-usart.c:40:32: error: ‘stm32f4_info’ defined but not used [-Werror=unused-variable]
static struct stm32_usart_info stm32f4_info = {
^~~~~~~~~~~~
cc1: all warnings being treated as errors
Mark these variables as __maybe_unused to fix this.
Fixes: c7039ce904 ("serial: stm32: make info structs static to avoid sparse warnings")
Signed-off-by: Ren Zhijie <renzhijie2@huawei.com>
Link: https://lore.kernel.org/r/20220926025826.44145-1-renzhijie2@huawei.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The STM32 USART can control RS-485 Transmit Enable in hardware. Since
commit 7df5081cbf ("serial: stm32: Add RS485 RTS GPIO control"),
it can alternatively be controlled in software. That was done to allow
RS-485 even if the RTS pin is unavailable because it's pinmuxed to a
different function.
However the commit neglected to deassert Transmit Enable upon invocation
of the ->rs485_config() callback. Fix it.
Avoid forward declarations by moving stm32_usart_tx_empty(),
stm32_usart_rs485_rts_enable() and stm32_usart_rs485_rts_disable()
further up in the driver.
Fixes: 7df5081cbf ("serial: stm32: Add RS485 RTS GPIO control")
Cc: stable@vger.kernel.org # v5.9+
Cc: Marek Vasut <marex@denx.de>
Reviewed-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Link: https://lore.kernel.org/r/6059eab35dba394468335ef640df8b0050fd9dbd.1662886616.git.lukas@wunner.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There should be no reason to adjust old ktermios which is going to get
discarded anyway.
Reviewed-by: Andy Shevchenko <andy.shevchenko@gmail.com>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220816115739.10928-7-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Here is the big set of tty and serial driver changes for 6.0-rc1.
It was delayed from last week as I wanted to make sure the last commit
here got some good testing in linux-next and elsewhere as it seemed to
show up only late in testing for some reason.
Nothing major here, just lots of cleanups from Jiri and Ilpo to make the
tty core cleaner (Jiri) and the rs485 code simpler to use (Ilpo). Also
included in here is the obligatory n_gsm updates from Daniel Starke and
lots of tiny driver updates and minor fixes and tweaks for other smaller
serial drivers.
Full details are in the shortlog.
All of these have been in linux-next for a while with no reported
problems.
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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Merge tag 'tty-6.0-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty
Pull tty / serial driver updates from Greg KH:
"Here is the big set of tty and serial driver changes for 6.0-rc1.
It was delayed from last week as I wanted to make sure the last commit
here got some good testing in linux-next and elsewhere as it seemed to
show up only late in testing for some reason.
Nothing major here, just lots of cleanups from Jiri and Ilpo to make
the tty core cleaner (Jiri) and the rs485 code simpler to use (Ilpo).
Also included in here is the obligatory n_gsm updates from Daniel
Starke and lots of tiny driver updates and minor fixes and tweaks for
other smaller serial drivers.
All of these have been in linux-next for a while with no reported
problems"
* tag 'tty-6.0-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/tty: (186 commits)
tty: serial: qcom-geni-serial: Fix %lu -> %u in print statements
tty: amiserial: Fix comment typo
tty: serial: document uart_get_console()
tty: serial: serial_core, reformat kernel-doc for functions
Documentation: serial: link uart_ops properly
Documentation: serial: move GPIO kernel-doc to the functions
Documentation: serial: dedup kernel-doc for uart functions
Documentation: serial: move uart_ops documentation to the struct
dt-bindings: serial: snps-dw-apb-uart: Document Rockchip RV1126
serial: mvebu-uart: uart2 error bits clearing
tty: serial: fsl_lpuart: correct the count of break characters
serial: stm32: make info structs static to avoid sparse warnings
serial: fsl_lpuart: zero out parity bit in CS7 mode
tty: serial: qcom-geni-serial: Fix get_clk_div_rate() which otherwise could return a sub-optimal clock rate.
serial: 8250_bcm2835aux: Add missing clk_disable_unprepare()
tty: vt: initialize unicode screen buffer
serial: remove VR41XX serial driver
serial: 8250: lpc18xx: Remove redundant sanity check for RS485 flags
serial: 8250_dwlib: remove redundant sanity check for RS485 flags
dt_bindings: rs485: Correct delay values
...
The info structs are local only to the stm32-usart.c driver and are
triggering sparse warnings about being undecalred. Move these into
the main driver code and make them static to avoid the following
warnings:
drivers/tty/serial/stm32-usart.h:42:25: warning: symbol 'stm32f4_info' was not declared. Should it be static?
drivers/tty/serial/stm32-usart.h:63:25: warning: symbol 'stm32f7_info' was not declared. Should it be static?
drivers/tty/serial/stm32-usart.h:85:25: warning: symbol 'stm32h7_info' was not declared. Should it be static?
Signed-off-by: Ben Dooks <ben-linux@fluff.org>
Link: https://lore.kernel.org/r/20220721212430.453192-1-ben-linux@fluff.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Embed rs485_supported to uart_port to allow serial core to tweak it as
needed.
Reviewed-by: Lino Sanfilippo <l.sanfilippo@kunbus.com>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220704094515.6831-2-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The code lacks clearing of previous DEAT/DEDT values. Thus, changing
values on the fly results in garbage delays tending towards the maximum
value as more and more bits are ORed together. (Leaving RS485 mode
would have cleared the old values though).
Fixes: 1bcda09d29 ("serial: stm32: add support for RS485 hardware control mode")
Cc: stable <stable@kernel.org>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220627150753.34510-1-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
To be able to alter ADDRB within ->rs485_config(), take termios_rwsem
before calling ->rs485_config() and pass termios.
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220624204210.11112-5-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add CSIZE sanitization for unsupported CSIZE configurations. In
addition, if parity is asked for but CSx was unsupported, the sensible
result is CS8+parity which requires setting USART_CR1_M0 like with 9
bits.
Incorrect CSIZE results in miscalculation of the frame bits in
tty_get_char_size() or in its predecessor where the roughly the same
code is directly within uart_update_timeout().
Fixes: c8a9d04394 (serial: stm32: fix word length configuration)
Cc: Erwan Le Ray <erwan.leray@st.com>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220519081808.3776-9-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In case the RS485 mode is emulated using GPIO RTS, use the TC interrupt
to deassert the GPIO RTS, otherwise the GPIO RTS stays asserted after a
transmission ended and the RS485 cannot work.
Signed-off-by: Marek Vasut <marex@denx.de>
Cc: Alexandre Torgue <alexandre.torgue@foss.st.com>
Cc: Erwan Le Ray <erwan.leray@foss.st.com>
Cc: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Cc: Jean Philippe Romain <jean-philippe.romain@foss.st.com>
Cc: Valentin Caron <valentin.caron@foss.st.com>
Cc: linux-arm-kernel@lists.infradead.org
Cc: linux-stm32@st-md-mailman.stormreply.com
To: linux-serial@vger.kernel.org
Link: https://lore.kernel.org/r/20220430162845.244655-2-marex@denx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Pull out the GPIO RTS enable and disable handling into separate function.
Limit the scope of GPIO RTS toggling only to GPIO emulated RS485 too.
Signed-off-by: Marek Vasut <marex@denx.de>
Cc: Alexandre Torgue <alexandre.torgue@foss.st.com>
Cc: Erwan Le Ray <erwan.leray@foss.st.com>
Cc: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Cc: Jean Philippe Romain <jean-philippe.romain@foss.st.com>
Cc: Valentin Caron <valentin.caron@foss.st.com>
Cc: linux-arm-kernel@lists.infradead.org
Cc: linux-stm32@st-md-mailman.stormreply.com
To: linux-serial@vger.kernel.org
Link: https://lore.kernel.org/r/20220430162845.244655-1-marex@denx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add support for KGDB in stm32 serial driver by implementing characters
polling callbacks (poll_init, poll_get_char and poll_put_char).
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Signed-off-by: Jean Philippe Romain <jean-philippe.romain@foss.st.com>
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Link: https://lore.kernel.org/r/20220419085330.1178925-3-valentin.caron@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Rework stm32_usart_console_putchar() function in order to anticipate
the case where the character can never be sent.
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Link: https://lore.kernel.org/r/20220419085330.1178925-2-valentin.caron@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In uart_set_rs485_config() the serial core already ensures that only one of
both options RTS on send or RTS after send is set. It also assigns the
passed serial_rs485 struct to the uart port.
So remove the check and the assignment from the drivers rs485_config()
function to avoid redundancy.
Signed-off-by: Lino Sanfilippo <LinoSanfilippo@gmx.de>
Link: https://lore.kernel.org/r/20220410104642.32195-4-LinoSanfilippo@gmx.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Currently, uart_console_write->putchar's second parameter (the
character) is of type int. It makes little sense, provided uart_console_write()
accepts the input string as "const char *s" and passes its content -- the
characters -- to putchar(). So switch the character's type to unsigned
char.
We don't use char as that is signed on some platforms. That would cause
troubles for drivers which (implicitly) cast the char to u16 when
writing to the device. Sign extension would happen in that case and the
value written would be completely different to the provided char. DZ is
an example of such a driver -- on MIPS, it uses u16 for dz_out in
dz_console_putchar().
Note we do the char -> uchar conversion implicitly in
uart_console_write(). Provided we do not change size of the data type,
sign extension does not happen there, so the problem is void.
This makes the types consistent and unified with the rest of the uart
layer, which uses unsigned char in most places already. One exception is
xmit_buf, but that is going to be converted later.
Cc: Paul Cercueil <paul@crapouillou.net>
Cc: Tobias Klauser <tklauser@distanz.ch>
Cc: Russell King <linux@armlinux.org.uk>
Cc: Vineet Gupta <vgupta@kernel.org>
Cc: Nicolas Ferre <nicolas.ferre@microchip.com>
Cc: Alexandre Belloni <alexandre.belloni@bootlin.com>
Cc: Ludovic Desroches <ludovic.desroches@microchip.com>
Cc: Florian Fainelli <f.fainelli@gmail.com>
Cc: bcm-kernel-feedback-list@broadcom.com
Cc: Alexander Shiyan <shc_work@mail.ru>
Cc: Baruch Siach <baruch@tkos.co.il>
Cc: "Maciej W. Rozycki" <macro@orcam.me.uk>
Cc: Paul Walmsley <paul.walmsley@sifive.com>
Cc: Palmer Dabbelt <palmer@dabbelt.com>
Cc: Albert Ou <aou@eecs.berkeley.edu>
Cc: Shawn Guo <shawnguo@kernel.org>
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Cc: Pengutronix Kernel Team <kernel@pengutronix.de>
Cc: Fabio Estevam <festevam@gmail.com>
Cc: NXP Linux Team <linux-imx@nxp.com>
Cc: Karol Gugala <kgugala@antmicro.com>
Cc: Mateusz Holenko <mholenko@antmicro.com>
Cc: Vladimir Zapolskiy <vz@mleia.com>
Cc: Neil Armstrong <narmstrong@baylibre.com>
Cc: Kevin Hilman <khilman@baylibre.com>
Cc: Jerome Brunet <jbrunet@baylibre.com>
Cc: Martin Blumenstingl <martin.blumenstingl@googlemail.com>
Cc: Taichi Sugaya <sugaya.taichi@socionext.com>
Cc: Takao Orito <orito.takao@socionext.com>
Cc: Liviu Dudau <liviu.dudau@arm.com>
Cc: Sudeep Holla <sudeep.holla@arm.com>
Cc: Lorenzo Pieralisi <lorenzo.pieralisi@arm.com>
Cc: "Andreas Färber" <afaerber@suse.de>
Cc: Manivannan Sadhasivam <mani@kernel.org>
Cc: Michael Ellerman <mpe@ellerman.id.au>
Cc: Benjamin Herrenschmidt <benh@kernel.crashing.org>
Cc: Paul Mackerras <paulus@samba.org>
Cc: Andy Gross <agross@kernel.org>
Cc: Bjorn Andersson <bjorn.andersson@linaro.org>
Cc: Krzysztof Kozlowski <krzysztof.kozlowski@canonical.com>
Cc: Orson Zhai <orsonzhai@gmail.com>
Cc: Baolin Wang <baolin.wang7@gmail.com>
Cc: Chunyan Zhang <zhang.lyra@gmail.com>
Cc: Patrice Chotard <patrice.chotard@foss.st.com>
Cc: Maxime Coquelin <mcoquelin.stm32@gmail.com>
Cc: Alexandre Torgue <alexandre.torgue@foss.st.com>
Cc: "David S. Miller" <davem@davemloft.net>
Cc: Peter Korsgaard <peter@korsgaard.com>
Cc: Michal Simek <michal.simek@xilinx.com>
Acked-by: Richard Genoud <richard.genoud@gmail.com> [atmel_serial]
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Acked-by: Paul Cercueil <paul@crapouillou.net>
Acked-by: Neil Armstrong <narmstrong@baylibre.com> # meson_serial
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Link: https://lore.kernel.org/r/20220303080831.21783-1-jslaby@suse.cz
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Enable mctrl_gpio wake_irq if device_may_wakeup when usart is suspended,
and disable mctrl_gpios wake_irq if device_may_wakeup when usart is
resumed.
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Link: https://lore.kernel.org/r/20220203171644.12231-3-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
x_char is ignored by stm32_usart_start_tx() when xmit buffer is empty.
Fix start_tx condition to allow x_char to be sent.
Fixes: 48a6092fb4 ("serial: stm32-usart: Add STM32 USART Driver")
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Link: https://lore.kernel.org/r/20220111164441.6178-3-valentin.caron@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When sending x_char in stm32_usart_transmit_chars(), driver can overwrite
the value of TDR register by the value of x_char. If this happens, the
previous value that was present in TDR register will not be sent through
uart.
This code checks if the previous value in TDR register is sent before
writing the x_char value into register.
Fixes: 48a6092fb4 ("serial: stm32-usart: Add STM32 USART Driver")
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Link: https://lore.kernel.org/r/20220111164441.6178-2-valentin.caron@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In this error handling, "transmit_chars_dma" function will call
"transmit_chars_pio" once per characters. But "transmit_chars_pio" will
continue to send characters while xmit buffer is not empty.
Remove this useless loop, one call is sufficient.
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Link: https://lore.kernel.org/r/20220104182445.4195-5-valentin.caron@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If flow control is enabled, framework will call stop_tx to
pause transfer and then call start_tx to resume transfer.
Clear USART_CR3_DMAT bit in stop_tx ops to pause DMA transfer.
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Link: https://lore.kernel.org/r/20220104182445.4195-4-valentin.caron@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
TX DMA state condition is handled by tx_dma_busy boolean.
This boolean is set when dma descriptor is requested and reset when dma
channel is stopped (dma_terminate).
In stm32_usart_serial_remove(), stm32_usart_stop_tx() and
stm32_usart_transmit_chars_dma() fallback error case, DMA channel is
stopped but tx_dma_busy is not handled.
Rework the driver by using two new functions to solve this issue:
- stm32_usart_tx_dma_started return true if DMA TX have a descriptor.
- stm32_usart_tx_dma_enabled return true if DMAT bit is set.
stm32_usart_tx_dma_started uses tx_dma_busy flag to prevent dual DMA
transaction at the same time. This flag is set when a DMA transaction
begins and is unset when dmaengine_terminate_async function is called.
A new DMA transaction cannot be created if this flag is set.
Create a new function "stm32_usart_tx_dma_terminate" to be sure the flag
is unset after each call of dmaengine_terminate_async.
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Link: https://lore.kernel.org/r/20220104182445.4195-3-valentin.caron@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Terminate DMA transaction and clear CR3_DMAT when shutdown is requested,
instead of when remove is requested. If DMA transfer is not stopped in
shutdown ops, driver will fail to start a new DMA transfer after next
startup ops.
Fixes: 3489187204 ("serial: stm32: adding dma support")
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Link: https://lore.kernel.org/r/20220104182445.4195-2-valentin.caron@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Data may be stored in DMA RX buffer, when suspending. The data needs
to be pushed to the upper layer. We can't rely on the timeout IRQ (RTOR)
that can't be triggered into low power state. So safely clear DMA request
(DMAR), force the DMA reception routines to push RX buffer content, before
disabling RX DMA. This way, handover to pio mode is safe.
Only call tty_flip_buffer_push() when there is RX data to handle.
Move the locking outside of stm32_usart_receive_chars() to prevent a race
condition, when disabling DMA request upon suspend / pm_runtime_suspend.
Data may be received under IRQ and pushed before
stm32_usart_receive_chars() has pushed older data from DMA rx_buf upon
suspend.
The sequence in suspend routine needs proper locking to avoid this.
Signed-off-by: Fabrice Gasnier <fabrice.gasnier@foss.st.com>
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Link: https://lore.kernel.org/r/20211025134229.8456-4-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
DMA prevents the system to suspend when an UART RX wake-up source is
using DMA. DMA can't suspend while DMA channels are still active.
Terminate DMA transfer at suspend, and restart a new DMA transfer at
resume. Create stm32_usart_start_rx_dma_cyclic function to factorize
dma RX initialization. Move RX DMA code related to wakeup into
stm32_usart_serial_en_wakeup() routine to ease further improvements
on wakeup from low power modes.
Don't enable/disable wakeup on uninitialized port.
There may be data residue in the RX FIFO while suspending. Flush it at
suspend time. Receiver timeout interrupt won't trigger later in low power
mode, so call stm32_usart_receive_chars() in case there's data to handle.
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Link: https://lore.kernel.org/r/20211025134229.8456-3-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The RX DMA channel is kept active forever (from the probe). That prevents
going to low power mode when it is used. This change moves the
DMA configuration and enabling procedures to startup routine to allow
transition to low power mode.
The DMA disabling procedure is implemented in stop_rx routine as this
ops has to stop characters reception, and DMA transation in shutdown.
Clean useless dma_async_tx_descriptor initialization to NULL value.
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Link: https://lore.kernel.org/r/20211025134229.8456-2-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Disable DMA request line (if enabled) to switch in PIO mode in throttle
ops, so the RX data gets queues into the FIFO. The hardware flow control
is triggered when the RX FIFO is full.
Switch back to DMA mode (re-enable DMA request line) in unthrottle ops.
Hardware flow control is stopped when FIFO is not full anymore.
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Link: https://lore.kernel.org/r/20211020150332.10214-4-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This patch reworks RX support over DMA to improve reliability:
- change dma buffer cyclic configuration by using 2 periods. DMA buffer
data are handled by a flip-flop between the 2 periods in order to avoid
risk of data loss/corruption
- change the size of dma buffer to 4096 to limit overruns
- add rx errors management (breaks, parity, framing and overrun).
When an error occurs on the uart line, the dma request line is masked at
HW level. The SW must 1st clear DMAR (dma request line enable), to
handle the error, then re-enable DMAR to recover. So, any correct data
is taken from the DMA buffer, before handling the error itself. Then
errors are handled from RDR/ISR/FIFO (e.g. in PIO mode). Last, DMA
reception is resumed.
- add a condition on DMA request line in DMA RX routines in order to
switch to PIO mode when no DMA request line is disabled, even if the DMA
channel is still enabled.
When the UART is wakeup source and is configured to use DMA for RX, any
incoming data that wakes up the system isn't correctly received.
At data reception, the irq_handler handles the WUF irq, and then the
data reception over DMA.
As the DMA transfer has been terminated at suspend, and will be restored
by resume callback (which has no yet been called by system), the data
can't be received.
The wake-up data has to be handled in PIO mode while suspend callback
has not been called.
Signed-off-by: Valentin Caron <valentin.caron@foss.st.com>
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Link: https://lore.kernel.org/r/20211020150332.10214-3-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Re-introduce an irq flag condition in usart_receive_chars.
This condition has been deleted by commit 75f4e830fa ("serial: do not
restore interrupt state in sysrq helper").
This code was present to handle threaded case, and has been removed
because it is no more needed in this case. Nevertheless an irq safe lock
is still needed in some cases, when DMA should be stopped to receive errors
or breaks in PIO mode.
This patch is a precursor to the complete rework or stm32 serial driver
DMA implementation.
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Link: https://lore.kernel.org/r/20211020150332.10214-2-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Use the defined variable 'dev' to make the code cleaner.
Signed-off-by: Zhang Shengju <zhangshengju@cmss.chinamobile.com>
Signed-off-by: Tang Bin <tangbin@cmss.chinamobile.com>
Link: https://lore.kernel.org/r/20210814124951.30084-1-tangbin@cmss.chinamobile.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In the function stm32_usart_init_port, intent of the code maybe when
irq returns a value of zero, the return should be '-ENODEV'. But the
conditional expression '? :' maybe clerical error, it should be
'?:' to make '-ENODEV' work.
But in fact, as the example in platform.c is
* int irq = platform_get_irq(pdev, 0);
* if (irq < 0)
* return irq;
So the return value of zero is unnecessary to check, at last remove
the unnecessary '?: -ENODEV'.
Co-developed-by: Zhang Shengju <zhangshengju@cmss.chinamobile.com>
Signed-off-by: Zhang Shengju <zhangshengju@cmss.chinamobile.com>
Signed-off-by: Tang Bin <tangbin@cmss.chinamobile.com>
Link: https://lore.kernel.org/r/20210811105136.25392-1-tangbin@cmss.chinamobile.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In the previous patch, we introduced tty_get_char_size() and
tty_get_frame_size() for computing character and frame sizes,
respectively. Here, we make use of them in various tty drivers where
applicable.
The stats look nice: 12 insertions, 169 deletions.
Cc: Arnd Bergmann <arnd@arndb.de>
Cc: David Lin <dtwlin@gmail.com>
Cc: Johan Hovold <johan@kernel.org>
Cc: Alex Elder <elder@kernel.org>
Cc: Shawn Guo <shawnguo@kernel.org>
Cc: Sascha Hauer <s.hauer@pengutronix.de>
Cc: Andy Gross <agross@kernel.org>
Cc: Bjorn Andersson <bjorn.andersson@linaro.org>
Cc: Maxime Coquelin <mcoquelin.stm32@gmail.com>
Cc: Alexandre Torgue <alexandre.torgue@foss.st.com>
Cc: Oliver Neukum <oneukum@suse.com>
Acked-by: Alex Elder <elder@kernel.org>
Signed-off-by: Jiri Slaby <jslaby@suse.cz>
Link: https://lore.kernel.org/r/20210610090247.2593-4-jslaby@suse.cz
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Defer device probe operation when a DMA channel request probe deferral.
With this change both DMA channels are acquired before DMA channels are
configured. Once no probe deferral is expected, DMAs are
configured and any failure in their configuration will make the driver
to fallback to interrupt mode as prior this change.
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Signed-off-by: Etienne Carriere <etienne.carriere@foss.st.com>
Link: https://lore.kernel.org/r/20210610100020.2318-1-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
There's no need to initialise irq-flags variables before saving the
interrupt state.
Drop the redundant initialisations from drivers that got this wrong.
Acked-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Johan Hovold <johan@kernel.org>
Link: https://lore.kernel.org/r/20210519092541.10137-1-johan@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add the support for two optional DT properties, to configure RX and TX
FIFO thresholds:
- rx-threshold
- tx-threshold
This replaces hard-coded 8 bytes threshold. Keep 8 as the default value if
not specified, for backward compatibility.
Signed-off-by: Fabrice Gasnier <fabrice.gasnier@foss.st.com>
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Changes in v2:
Change added properties naming as proposed by Rob Herring.
Link: https://lore.kernel.org/r/20210413174015.23011-5-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Use the uart_unlock_and_check_sysrq() helper to defer sysrq processing
until receive processing is done and the port lock has been released.
This allows cleaning up the console_write() implementation by not having
to work around the recursive sysrq case (by dropping locking completely)
and also makes the console code work with PREEMPT_RT by no longer
relying on local_irq_save().
Reviewed-by: Valentin Caron<valentin.caron@foss.st.com>
Signed-off-by: Johan Hovold <johan@kernel.org>
Link: https://lore.kernel.org/r/20210416140557.25177-4-johan@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When DMA is enabled the receive handler runs in a threaded handler, but
the primary handler up until very recently neither disabled interrupts
in the device or used IRQF_ONESHOT. This would lead to a deadlock if an
interrupt comes in while the threaded receive handler is running under
the port lock.
Commit ad76768124 ("serial: stm32: fix a deadlock condition with
wakeup event") claimed to fix an unrelated deadlock, but unfortunately
also disabled interrupts in the threaded handler. While this prevents
the deadlock mentioned in the previous paragraph it also defeats the
purpose of using a threaded handler in the first place.
Fix this by making the interrupt one-shot and not disabling interrupts
in the threaded handler.
Note that (receive) DMA must not be used for a console port as the
threaded handler could be interrupted while holding the port lock,
something which could lead to a deadlock in case an interrupt handler
ends up calling printk.
Fixes: ad76768124 ("serial: stm32: fix a deadlock condition with wakeup event")
Fixes: 3489187204 ("serial: stm32: adding dma support")
Cc: stable@vger.kernel.org # 4.9
Cc: Alexandre TORGUE <alexandre.torgue@st.com>
Cc: Gerald Baeza <gerald.baeza@st.com>
Reviewed-by: Valentin Caron<valentin.caron@foss.st.com>
Signed-off-by: Johan Hovold <johan@kernel.org>
Link: https://lore.kernel.org/r/20210416140557.25177-3-johan@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The wakeup specific IRQ management is no more needed to wake up the stm32
plaform. A relationship has been established between the EXTI and
the EVENT IRQ, just need to declare the EXTI interrupt instead of the
UART event IRQ.
Signed-off-by: Alexandre Torgue <alexandre.torgue@foss.st.com>
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Link: https://lore.kernel.org/r/20210319184253.5841-5-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Remove useless call to stm32_usart_serial_en_wakeup() routine in suspend
callback. When called with "false" argument, this routine is clearing UESM
and WUFIE bits if usart is not wakeup source. Those bits are already
cleared in set_termios(), and then in serial_resume() callback when usart
is wakeup source.
Signed-off-by: Alexandre Torgue <alexandre.torgue@foss.st.com>
Signed-off-by: Erwan Le Ray <erwan.leray@foss.st.com>
Link: https://lore.kernel.org/r/20210319184253.5841-3-erwan.leray@foss.st.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>