The fifo memory allocation in mode_2_cfg[] doesn't utilize all the 4KB
memory.
Increse some endpoint fifo buffers to fully use all the 4KB memory. Now
we can support more webcam usecases on DA8xx.
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
For tusb6010 the DMA functionality only possible if the buffer is 32bit
aligned (SYNC access to FIFO) since with ASYNC access the TX/RX offset
registers will corrupt eventually.
The MUSB_G_NO_SKB_RESERVE will set the quirk_avoids_skb_reserve flag in
usb_gadget struct to provide correctly aligned buffer.
Signed-off-by: Peter Ujfalusi <peter.ujfalusi@ti.com>
Tested-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
In the DA8xx, USB and CPPI 4.1 are sharing the same interrupt line.
Update the driver to request a shared irq.
Signed-off-by: Alexandre Bailon <abailon@baylibre.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add code comment to make it clear that the fall-through is intentional.
Read the link for more details: https://lkml.org/lkml/2017/2/9/292
Addresses-Coverity-ID: 1397608
Signed-off-by: Gustavo A. R. Silva <garsilva@embeddedor.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
On da8xx, VBUS is not maintained during suspend when musb is in host mode.
On resume, all the connected devices will be disconnected and then will
be enumerated again.
This happens because MUSB_DEVCTL is cleared during suspend.
Add a quirk to not clear MUSB_DEVCTL and then preserve the session during
a suspend.
Signed-off-by: Alexandre Bailon <abailon@baylibre.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
musb_generic_disable() only has two lines of code. So remove it and let
the callers directly call those two lines.
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
While testing musb host mode cable plugging on a BeagleBone, I came across this
error:
Unhandled fault: external abort on non-linefetch (0x1008) at 0xd1dcfc60
...
[<bf668390>] (musb_default_readb [musb_hdrc]) from [<bf668578>] (musb_irq_work+0x1c/0x180 [musb_hdrc])
[<bf668578>] (musb_irq_work [musb_hdrc]) from [<c0156554>] (process_one_work+0x2b4/0x808)
[<c0156554>] (process_one_work) from [<c015767c>] (worker_thread+0x3c/0x550)
[<c015767c>] (worker_thread) from [<c015d568>] (kthread+0x104/0x148)
[<c015d568>] (kthread) from [<c01078d0>] (ret_from_fork+0x14/0x24)
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Commit 467d5c9807 ("usb: musb: Implement session bit based runtime PM for
musb-core") started implementing musb generic runtime PM support by
introducing devctl register session bit based state control.
This caused a regression where if a USB mass storage device is connected
to a USB hub, we can get:
usb 1-1: reset high-speed USB device number 2 using musb-hdrc
usb 1-1: device descriptor read/64, error -71
usb 1-1.1: new high-speed USB device number 4 using musb-hdrc
This is because before the USB storage device is connected, musb is
in OTG_STATE_A_SUSPEND. And we currently only set need_finish_resume
in musb_stage0_irq() and the related code calling finish_resume_work
in musb_resume() and musb_runtime_resume() never gets called.
To fix the issue, we can call schedule_delayed_work() directly in
musb_stage0_irq() to have finish_resume_work run.
And we should no longer never get interrupts when when suspended.
We have changed musb to no longer need pm_runtime_irqsafe().
The need_finish_resume flag was added in commit 9298b4aad3 ("usb:
musb: fix device hotplug behind hub") and no longer applies as far
as I can tell. So let's just remove the earlier code that no longer
is needed.
Fixes: 467d5c9807 ("usb: musb: Implement session bit based runtime PM for musb-core")
Reported-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The function musb_run_resume_work is called only when CONFIG_PM is
enabled. So this function should not be defined when CONFIG_PM is
disabled. Otherwise the compiler issues a warning:
drivers/usb/musb/musb_core.c:2057:12: error: ‘musb_run_resume_work’ defined but
not used [-Werror=unused-function]
static int musb_run_resume_work(struct musb *musb)
^~~~~~~~~~~~~~~~~~~~
Signed-off-by: Jérémy Lefaure <jeremy.lefaure@lse.epita.fr>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This adds the function musb_get_mode() to get the DT property "dr_mode"
Signed-off-by: Petr Kulhavy <petr@barix.com>
Acked-by: Sergei Shtylyov <sshtylyov@ru.mvista.com>
Signed-off-by: Alexandre Bailon <abailon@baylibre.com>
Tested-by: David Lechner <david@lechnology.com>
Reviewed-by: Kevin Hilman <khilman@baylibre.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Don't complain on -EPROBE_DEFER when initializing controller,
the driver probe will be retried later.
Signed-off-by: Ladislav Michl <ladis@linux-mips.org>
Acked-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Remove comments about resume signalling being stopped from
GetPortStatus, something which is no longer the case.
Fixes: 8ed1fb790e ("usb: musb: finish suspend/reset work...")
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
With a USB hub disconnected, devctl can be 0x19 for about a second
on am335x and will stay forever on at least omap3. And we get no
further interrupts when devctl session bit clears. This keeps
PM runtime active.
Let's fix the issue by polling devctl until the session bit clears
or times out. We can do this by making musb->irq_work into
delayed_work.
And with the polling implemented, we can now also have the quirk
for invalid VBUS it to avoid disconnecting too early while VBUS
is ramping up.
Fixes: 467d5c9807 ("usb: musb: Implement session bit based runtime
PM for musb-core")
Fixes: 65b3f50ed6 ("usb: musb: Add PM runtime support for MUSB DSPS
Tested-by: Ladislav Michl <ladis@linux-mips.org>
Tested-by: Laurent Pinchart <laurent.pinchart@ideasonboard.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Commit 65b3f50ed6 ("usb: musb: Add PM runtime support for MUSB DSPS
glue layer") wrongly added a call for pm_runtime_get_sync to otg_timer
that runs in softirq context. That causes a "BUG: sleeping function called
from invalid context" every time when polling the cable status:
[<c015ebb4>] (__might_sleep) from [<c0413d60>] (__pm_runtime_resume+0x9c/0xa0)
[<c0413d60>] (__pm_runtime_resume) from [<c04d0bc4>] (otg_timer+0x3c/0x254)
[<c04d0bc4>] (otg_timer) from [<c0191180>] (call_timer_fn+0xfc/0x41c)
[<c0191180>] (call_timer_fn) from [<c01915c0>] (expire_timers+0x120/0x210)
[<c01915c0>] (expire_timers) from [<c0191acc>] (run_timer_softirq+0xa4/0xdc)
[<c0191acc>] (run_timer_softirq) from [<c010168c>] (__do_softirq+0x12c/0x594)
I did not notice that as I did not have CONFIG_DEBUG_ATOMIC_SLEEP enabled.
And looks like also musb_gadget_queue() suffers from the same problem.
Let's fix the issue by using a list of delayed work then call it on
resume. Note that we want to do this only when musb core and it's
parent devices are awake, and we need to make sure the DSPS glue
timer is stopped as noted by Johan Hovold <johan@kernel.org>.
Note that we already are re-enabling the timer with mod_timer() in
dsps_musb_enable().
Later on we may be able to remove other delayed work in the musb driver
and just do it from pending_resume_work. But this should be done only
for delayed work that does not have other timing requirements beyond
just being run on resume.
Fixes: 65b3f50ed6 ("usb: musb: Add PM runtime support for MUSB DSPS
glue layer")
Reported-by: Johan Hovold <johan@kernel.org>
Reviewed-by: Johan Hovold <johan@kernel.org>
Tested-by: Laurent Pinchart <laurent.pinchart@ideasonboard.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
We can't use static variable first for checking when musb is
initialized when we have multiple musb instances like on am335x.
Tested-by: Ladislav Michl <ladis@linux-mips.org>
Reviewed-by: Johan Hovold <johan@hovoldconsulting.com>
Tested-by: Laurent Pinchart <laurent.pinchart@ideasonboard.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
With the session bit based PM runtime working on musb, we've
implemented few quirks to attempt to detect the current state of
the hardware. One of the quirks is for invalid VBUS as peripheral,
but it is not working in all cases.
If we start musb on dm3730 as a peripheral with no cable connected,
we will get the devctl 91 state once and will never idle as there
are not further interrupts from musb. So we need to ignore the first
devctl 91 state as there will be more interrupts if we're connected.
The invalid VBUS state also can happen always when connected to
certain USB hubs. Looks like musb on dm3730 can claim invalid VBUS
with some hubs while 3717-evm and BeagleBone don't. This causes
session as peripheral to fail for dm3730 with some hubs.
This too is fixed by ignoring only the first invalid VBUS. When
connected, we can just look at the session bit as that will clear
automatically when the session ends.
Fixes: 467d5c9807 ("usb: musb: Implement session bit based runtime PM for musb-core")
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
aDate is always the empty string, so entirely pointless. The aRevision
formatting might as well be done as part of the pr_debug() call - that
also avoids it altogether if pr_debug is compiled out.
Signed-off-by: Rasmus Villemoes <linux@rasmusvillemoes.dk>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
We want to keep musb enabled always when the session bit is
set. This simplifies the PM runtime and allows making it more
generic across the various glue layers.
So far the only exception to just following the session bit is
host mode disconnect where the session bit stays set.
In that case, just allow PM and let the PM runtime autoidle
timeout deal with it.
Signed-off-by: Tony Lindgren <tony@atomide.com>
[b-liu@ti.com: changed using dev_dbg() to musb_dbg()]
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This adds tracepoints to dump musb interrupt events.
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This adds tracepoints to musb register read/write wrappers to get
trace log for register access.
The default tacepoint log prefix here would be musb_readX/writeX(),
which is not much helpful. So this patch let the tracepoints use
__buildin_return_address(0) to print the caller funciton name to
provide more context of the register access.
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
If the session bit was not set in the backup of devctl register,
restoring devctl would clear the session bit. Therefor, only restore
devctl register when the session bit was set in the backup.
This solves the device enumeration failure in otg mode exposed by commit
56f487c (PM / Runtime: Update last_busy in rpm_resume).
Cc: <stable@vger.kernel.org> # v4.2+
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
With the pull up being handled with delayed work, we can
now finally remove pm_runtime_set_irq_safe that blocks the
MUSB glue from idling.
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
At least on n900 we have phy-twl4030-usb only generating cable
interrupts, and then have a separate USB PHY.
In order for musb to know the real cable status, we need to
clear any cached state until musb is ready. Otherwise the cable
status interrupts will get just ignored if the status does
not change from the initial state.
To do this, let's add a return value to musb_mailbox(), and
reset cached linkstat to MUSB_UNKNOWN on error. Sorry to cause
a bit of churn here, I should have added that already last time
patching musb_mailbox().
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Let's not tinker with the PM runtime of musb core from the omap2430
wrapper. This allows us to initialize PM runtime for musb core later
on instead of doing it in stages. And omap2430 wrapper has no need
to for accessing musb core at this point.
Note that this does not remove all the PM runtime calls from the
glue layer, those will get removed in a later patch.
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Let's make the PM runtime use the standard autosuspend calls.
Commit 5de85b9d57 ("PM / runtime: Re-init runtime PM states at probe
error and driver unbind") means we must pair use_autosuspend with
dont_use_autosuspend and then use put_sync to properly idle the
device.
Note that we'll be removing the PM runtime calls from the glue
layer to the MUSB core in the next patch. And we can also remove
the pointless FIXME comment now.
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
We have remove() already calling shutdown(), so let's drop it
and move the code to remove(). No code changes, we'll drop the
the FIXME in the following patch with more clean-up.
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Looks like at least 2430 glue won't idle reliably with the 200 ms
autosuspend delay. This causes deeper idle states being blocked for
the whole SoC when disconnecting OTG A cable.
Increasing the delay to 500 ms seems to idle both MUSB and the PHY
reliably. This is probably because of time needed by the hardware
based negotiation between MUSB and the PHY.
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The musb_hdrc_platform_data::config was defined as a non-const pointer.
However some drivers (e.g. the ux500) set up this pointer to point to a
static structure, which is potentially dangerous. Since the musb core
uses the pointer in a read-only manner the const qualifier was added to
protect the content of the config.
Signed-off-by: Petr Kulhavy <petr@barix.com>
Acked-by: Sergei Shtylyov <sergei.shtylyov@cogentembedded.com>
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Felipe Balbi <balbi@kernel.org>
The phy's init routine must be called before it can be used. Do so in
musb_init_controller and the matching shutdown in musb_remove.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Felipe Balbi <balbi@ti.com>
We currently can't unload omap2430 MUSB platform glue driver module and
this cause issues for fixing the MUSB code further. The reason we can't
remove omap2430 is because it uses the PHY functions and also exports the
omap_musb_mailbox function that some PHY drivers are using.
Let's fix the issue by exporting a more generic musb_mailbox function
from the MUSB core and allow platform glue layers to register phy_callback
function as needed.
And now we can now also get rid of the include/linux/musb-omap.h.
Cc: Bin Liu <b-liu@ti.com>
Cc: Felipe Balbi <balbi@ti.com>
Cc: Kishon Vijay Abraham I <kishon@ti.com>
Cc: NeilBrown <neil@brown.name>
Reviewed-by: Kishon Vijay Abraham I <kishon@ti.com>
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
This file already uses pr_debug in a few places; this converts the
remaining printks.
Signed-off-by: Rasmus Villemoes <linux@rasmusvillemoes.dk>
Signed-off-by: Felipe Balbi <balbi@ti.com>
If musb_init_controller fails at musb_platform_init, we have already
called pm_runtime_irq_safe for musb and that causes the pm runtime count
to be enabled for parent before the parent has completed initialization.
This causes pm to stop working as on unload nothing gets idled.
This issue can be reproduced at least with:
# modprobe omap2430
HS USB OTG: no transceiver configured
musb-hdrc musb-hdrc.0.auto: musb_init_controller failed with status -517
# modprobe phy-twl4030-usb
# rmmod omap2430
And after the steps above omap2430 will block deeper idle states on
omap3.
To fix this, let's not enable pm runtime until we need to and the
parent has been initialized. Note that this does not fix the issue of
PM being broken for musb during runtime.
Signed-off-by: Tony Lindgren <tony@atomide.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
Change the permission of usb_dma parameter so it can
be used for runtime debug without reboot.
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
There is a bit of a mess in the order of arguments to the ulpi write
callback. There is
int ulpi_write(struct ulpi *ulpi, u8 addr, u8 val)
in drivers/usb/common/ulpi.c;
struct usb_phy_io_ops {
...
int (*write)(struct usb_phy *x, u32 val, u32 reg);
}
in include/linux/usb/phy.h.
The callback registered by the musb driver has to comply to the latter,
but up to now had "offset" first which effectively made the function
broken for correct users. So flip the order and while at it also
switch to the parameter names of struct usb_phy_io_ops's write.
Fixes: ffb865b1e4 ("usb: musb: add ulpi access operations")
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Felipe Balbi <balbi@ti.com>
Fix musb_platform_get_vbus_status return value in case of platform
implementation is not defined, bringing expected behaviour of
musb_platform_get wrapper. Add musb_vbus_show default method to determine
VBUS status in case platform method is not defined.
Signed-off-by: Roman Alyautdin <ralyautdin@dev.rtsoft.ru>
Signed-off-by: Felipe Balbi <balbi@ti.com>
Set the Power register HSENAB bit based on musb->config->maximum_speed,
so that the glue layer can control MUSB to work in high- or full-speed.
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
In certain situations, an interrupt triggers on resume, before musb_start()
has been called. This has been observed to cause enumeration issues after
suspend/resume cycles with AM335x.
Signed-off-by: Pascal Huerst <pascal.huerst@gmail.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
The change ensures otg is not in a A- state when checking for VBUS in
peripheral mode.
musb_start() where VBUS checking is in can be called in many situations.
One example is in babble recovery routine, in which otg is transitioning
from A-HOST to A-WAIT-BCON, but VBUS discharge takes time, so
musb->is_active could be set to 1 due to this improper checking, then it
causes musb_bus_suspend() failed which leads to warning log message
flooding.
Signed-off-by: Bin Liu <b-liu@ti.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
This resolves a merge issue in musb_core.c and we want the fixes that
were in Linus's tree in this branch as well for testing.
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
musb-core was setting the ops to the default indexed or flat handlers after
checking for platform overrides. Reverse the order of this so that platform
overrides actually work.
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
The generic fifo functions already use non wrapped accesses in various
cases through the iowrite#_rep functions, and all platforms which override
the default musb_read[b|w] / _write[b|w] functions also provide their own
fifo access functions, so we can safely drop the unnecessary indirection
from the fifo access functions.
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
The Allwinner (sunxi) implementation of the musb has its busctl registers
indexed by the MUSB_INDEX register rather then in a flat address space.
This commit turns MUSB_BUSCTL_OFFSET from a macro into an io-op which can
be overridden from the platform ops.
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
For some reason the musb_write_rxfun* and musb_write_rxhub* functions had
a different function prototype and some extra magic needed on the caller side
compared to their tx counterparts, this commit makes them work the same as
their tx counterparts.
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Felipe Balbi <balbi@ti.com>
Currently we always assign one of the two common implementations of
ep_offset and ep_select operations, overwriting any platform-specific
implementations.
Fixes: d026e9c76a ("usb: musb: Change end point selection to use ...")
Signed-off-by: Ben Hutchings <ben@decadent.org.uk>
Signed-off-by: Felipe Balbi <balbi@ti.com>