It is wrong to use uninitialized dma_slave_config and configure only
certain fields as the DMAengine driver might look at non initialized
(random data) fields and tries to interpret it.
Signed-off-by: Peter Ujfalusi <peter.ujfalusi@ti.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Some ST platforms contain interconnect (ICN) clocks which must be handed
correctly in order to obtain full functionality of a given IP. In this
case, if the ICN clocks are not handled properly by the ST SDHCI driver
MMC will break and the following output can be observed:
[ 13.916949] mmc0: Timeout waiting for hardware interrupt.
[ 13.922349] sdhci: =========== REGISTER DUMP (mmc0)===========
[ 13.928175] sdhci: Sys addr: 0x00000000 | Version: 0x00001002
[ 13.933999] sdhci: Blk size: 0x00007040 | Blk cnt: 0x00000001
[ 13.939825] sdhci: Argument: 0x00fffff0 | Trn mode: 0x00000013
[ 13.945650] sdhci: Present: 0x1fff0206 | Host ctl: 0x00000011
[ 13.951475] sdhci: Power: 0x0000000f | Blk gap: 0x00000080
[ 13.957300] sdhci: Wake-up: 0x00000000 | Clock: 0x00003f07
[ 13.963126] sdhci: Timeout: 0x00000004 | Int stat: 0x00000000
[ 13.968952] sdhci: Int enab: 0x02ff008b | Sig enab: 0x02ff008b
[ 13.974777] sdhci: AC12 err: 0x00000000 | Slot int: 0x00000000
[ 13.980602] sdhci: Caps: 0x21ed3281 | Caps_1: 0x00000000
[ 13.986428] sdhci: Cmd: 0x0000063a | Max curr: 0x00000000
[ 13.992252] sdhci: Host ctl2: 0x00000000
[ 13.996166] sdhci: ADMA Err: 0x00000000 | ADMA Ptr: 0x7c048200
[ 14.001990] sdhci: ===========================================
[ 14.009802] mmc0: Got data interrupt 0x02000000 even though no data operation was in progress.
A decent point was raised about minimising the use of a local variable that
we 'could' do without. I've chosen consistency over the possibility of
reducing the local variable count by 1. Thinking that it's more important
for the code to be grouped and authoured in a similar manner/style for
greater maintainability/readability.
Cc: stable@vger.kernel.org
Tested-by: Peter Griffin <peter.griffin@linaro.org>
Signed-off-by: Lee Jones <lee.jones@linaro.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
- A couple of changes to improve the support for erase/discard/trim cmds
- Add eMMC HS400 enhanced strobe support
- Show OCR and DSR registers in SYSFS for MMC/SD cards
- Correct and improve busy detection logic for MMC switch (CMD6) cmds
- Disable HPI cmds for certain broken Hynix eMMC cards
- Allow MMC hosts to specify non-support for SD and MMC cmds
- Some minor additional fixes
MMC host:
- sdhci: Re-works, fixes and clean-ups
- sdhci: Add HW auto re-tuning support
- sdhci: Re-factor code to prepare for adding support for eMMC CMDQ
- sdhci-esdhc-imx: Fixes and clean-ups
- sdhci-esdhc-imx: Update system PM support
- sdhci-esdhc-imx: Enable HW auto re-tuning
- sdhci-bcm2835: Remove driver as sdhci-iproc is used instead
- sdhci-brcmstb: Add new driver for Broadcom BRCMSTB SoCs
- sdhci-msm: Add support for UHS cards
- sdhci-tegra: Improve support for UHS cards
- sdhci-of-arasan: Update phy support for Rockchip SoCs
- sdhci-of-arasan: Deploy enhanced strobe support
- dw_mmc: Some fixes and clean-ups
- dw_mmc: Enable support for erase/discard/trim cmds
- dw_mmc: Enable CMD23 support
- mediatek: Some fixes related to the eMMC HS400 support
- sh_mmcif: Improve support for HW busy detection
- rtsx_pci: Enable support for erase/discard/trim cmds
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Merge tag 'mmc-v4.8' of git://git.linaro.org/people/ulf.hansson/mmc
Pull MMC updates from Ulf Hansson:
"MMC core:
- A couple of changes to improve the support for erase/discard/trim cmds
- Add eMMC HS400 enhanced strobe support
- Show OCR and DSR registers in SYSFS for MMC/SD cards
- Correct and improve busy detection logic for MMC switch (CMD6) cmds
- Disable HPI cmds for certain broken Hynix eMMC cards
- Allow MMC hosts to specify non-support for SD and MMC cmds
- Some minor additional fixes
MMC host:
- sdhci: Re-works, fixes and clean-ups
- sdhci: Add HW auto re-tuning support
- sdhci: Re-factor code to prepare for adding support for eMMC CMDQ
- sdhci-esdhc-imx: Fixes and clean-ups
- sdhci-esdhc-imx: Update system PM support
- sdhci-esdhc-imx: Enable HW auto re-tuning
- sdhci-bcm2835: Remove driver as sdhci-iproc is used instead
- sdhci-brcmstb: Add new driver for Broadcom BRCMSTB SoCs
- sdhci-msm: Add support for UHS cards
- sdhci-tegra: Improve support for UHS cards
- sdhci-of-arasan: Update phy support for Rockchip SoCs
- sdhci-of-arasan: Deploy enhanced strobe support
- dw_mmc: Some fixes and clean-ups
- dw_mmc: Enable support for erase/discard/trim cmds
- dw_mmc: Enable CMD23 support
- mediatek: Some fixes related to the eMMC HS400 support
- sh_mmcif: Improve support for HW busy detection
- rtsx_pci: Enable support for erase/discard/trim cmds"
* tag 'mmc-v4.8' of git://git.linaro.org/people/ulf.hansson/mmc: (135 commits)
mmc: rtsx_pci: Remove deprecated create_singlethread_workqueue
mmc: rtsx_pci: Enable MMC_CAP_ERASE to allow erase/discard/trim requests
mmc: rtsx_pci: Use the provided busy timeout from the mmc core
mmc: sdhci-pltfm: Drop define for SDHCI_PLTFM_PMOPS
mmc: sdhci-pltfm: Convert to use the SET_SYSTEM_SLEEP_PM_OPS
mmc: sdhci-pltfm: Make sdhci_pltfm_suspend|resume() static
mmc: sdhci-esdhc-imx: Use common sdhci_suspend|resume_host()
mmc: sdhci-esdhc-imx: Assign system PM ops within #ifdef CONFIG_PM_SLEEP
mmc: sdhci-sirf: Remove non needed #ifdef CONFIG_PM* for dev_pm_ops
mmc: sdhci-s3c: Remove non needed #ifdef CONFIG_PM for dev_pm_ops
mmc: sdhci-pxav3: Remove non needed #ifdef CONFIG_PM for dev_pm_ops
mmc: sdhci-of-esdhc: Simplify code by using SIMPLE_DEV_PM_OPS
mmc: sdhci-acpi: Simplify code by using SET_SYSTEM_SLEEP_PM_OPS
mmc: sdhci-pci-core: Simplify code by using SET_SYSTEM_SLEEP_PM_OPS
mmc: Change the max discard sectors and erase response when HW busy detect
phy: rockchip-emmc: Wait even longer for the DLL to lock
phy: rockchip-emmc: Be tolerant to card clock of 0 in power on
mmc: sdhci-of-arasan: Revert: Always power the PHY off/on when clock changes
mmc: sdhci-msm: Add support for UHS cards
mmc: sdhci-msm: Add set_uhs_signaling() implementation
...
The workqueue "workq" provides support for sd/mmc async request, which
makes next request do dma_map_sg() while previous request transferring
data.
The workqueue has a single workitem(&host->work) and hence doesn't require
ordering. Also, it is not being used on a memory reclaim path. Hence,
the singlethreaded workqueue has been replaced with the use of system_wq.
System workqueues have been able to handle high level of concurrency
for a long time now and hence it's not required to have a singlethreaded
workqueue just to gain concurrency. Unlike a dedicated per-cpu workqueue
created with create_singlethread_workqueue(), system_wq allows multiple
work items to overlap executions even on the same CPU; however, a
per-cpu workqueue doesn't have any CPU locality or global ordering
guarantee unless the target CPU is explicitly specified and thus the
increase of local concurrency shouldn't make any difference.
Work item has been flushed in rtsx_pci_sdmmc_drv_remove() to ensure that
there are no pending tasks while disconnecting the driver.
Signed-off-by: Bhaktipriya Shridhar <bhaktipriya96@gmail.com>
Acked-by: Tejun Heo <tj@kernel.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The rtsx_pci driver is using a fixed 3s timeout for R1B responses, which
in some cases isn't suffient. For example, erase/discard requests may
require longer timeouts.
Instead of always using a fixed timeout, let's use the per request
calculated busy timeout from the mmc core.
Cc: Micky Ching <micky_ching@realsil.com.cn>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tested-by: Mauro Santos <registo.mailling@gmail.com>
Due to previous changes this define has no longer a purpose. Instead move
the sdhci-pltfm drivers over to use the exported struct sdhci_pltfm_pmops.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Move the system PM callbacks within #ifdef CONFIG_PM_SLEEP as to avoid
them being build when not used. This also allows us to use the
SET_SYSTEM_SLEEP_PM_OPS macro which simplifies the code.
Within this context it also makes sense to move the declaration of the
struct sdhci_pltfm_pmops, outside the #ifdef CONFIG_PM as the
SET_SYSTEM_SLEEP_PM_OPS deals with this. This further simplifies the code.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
To prepare to make the sdhci_pltfm_suspend|resume() static functions, move
sdhci-esdhc-imx over to use the sdhci_suspend|resume_host().
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Dong Aisheng <aisheng.dong@nxp.com>
The system PM callbacks isn't used unless CONFIG_PM_SLEEP is set, thus it
triggers a compiler warning about unused functions. Avoid this by changing
from CONFIG_PM to CONFIG_PM_SLEEP.
Reported-by: Arnd Bergmann <arnd@arndb.de>
Fixes: b70d0b3b5b29 ("mmc: sdhci-esdhc-imx: add esdhc specific suspend resume callback")
Cc: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Dong Aisheng <aisheng.dong@nxp.com>
The SIMPLE_DEV_PM_OPS macro deals with the CONFIG_PM options when
assigning the PM callbacks, thus it's not needed to control this when
using the macro. By removing the non needed #ifdef, the code becomes a
bit cleaner.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
As the SET_SYSTEM_SLEEP_PM_OPS and the SET_RUNTIME_PM_OPS macro deals with
the CONFIG_PM options when assigning the callbacks, it becomes redundant
to control this when declaring the struct dev_pm_ops. Instead let's always
declare it as it simplifies the code.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
As the SET_SYSTEM_SLEEP_PM_OPS and the SET_RUNTIME_PM_OPS macro deals with
the CONFIG_PM options when assigning the callbacks, it becomes redundant
to control this when declaring the struct dev_pm_ops. Instead let's always
declare it as it simplifies the code.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Let's use the SIMPLE_DEV_PM_OPS macro when declaring/assigning the system
PM callbacks, as the code gets simplified.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
By using the SET_SYSTEM_SLEEP_PM_OPS when assigning the system PM
callbacks, we can remove some #ifdefs so code becomes a bit cleaner.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Convert to define the system PM callbacks to be build for CONFIG_PM_SLEEP
and use the SET_SYSTEM_SLEEP_PM_OPS. In this way the code becomes cleaner.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Pull timer updates from Thomas Gleixner:
"This update provides the following changes:
- The rework of the timer wheel which addresses the shortcomings of
the current wheel (cascading, slow search for next expiring timer,
etc). That's the first major change of the wheel in almost 20
years since Finn implemted it.
- A large overhaul of the clocksource drivers init functions to
consolidate the Device Tree initialization
- Some more Y2038 updates
- A capability fix for timerfd
- Yet another clock chip driver
- The usual pile of updates, comment improvements all over the place"
* 'timers-core-for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/tip/tip: (130 commits)
tick/nohz: Optimize nohz idle enter
clockevents: Make clockevents_subsys static
clocksource/drivers/time-armada-370-xp: Fix return value check
timers: Implement optimization for same expiry time in mod_timer()
timers: Split out index calculation
timers: Only wake softirq if necessary
timers: Forward the wheel clock whenever possible
timers/nohz: Remove pointless tick_nohz_kick_tick() function
timers: Optimize collect_expired_timers() for NOHZ
timers: Move __run_timers() function
timers: Remove set_timer_slack() leftovers
timers: Switch to a non-cascading wheel
timers: Reduce the CPU index space to 256k
timers: Give a few structs and members proper names
hlist: Add hlist_is_singular_node() helper
signals: Use hrtimer for sigtimedwait()
timers: Remove the deprecated mod_timer_pinned() API
timers, net/ipv4/inet: Initialize connection request timers as pinned
timers, drivers/tty/mips_ejtag: Initialize the poll timer as pinned
timers, drivers/tty/metag_da: Initialize the poll timer as pinned
...
Pull x86 platform updates from Ingo Molnar:
"The main changes in this cycle were:
- Intel-SoC enhancements (Andy Shevchenko)
- Intel CPU symbolic model definition rework (Dave Hansen)
- ... other misc changes"
* 'x86-platform-for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/tip/tip: (25 commits)
x86/sfi: Enable enumeration of SD devices
x86/pci: Use MRFLD abbreviation for Merrifield
x86/platform/intel-mid: Make vertical indentation consistent
x86/platform/intel-mid: Mark regulators explicitly defined
x86/platform/intel-mid: Rename mrfl.c to mrfld.c
x86/platform/intel-mid: Enable spidev on Intel Edison boards
x86/platform/intel-mid: Extend PWRMU to support Penwell
x86/pci, x86/platform/intel_mid_pci: Remove duplicate power off code
x86/platform/intel-mid: Add pinctrl for Intel Merrifield
x86/platform/intel-mid: Enable GPIO expanders on Edison
x86/platform/intel-mid: Add Power Management Unit driver
x86/platform/atom/punit: Enable support for Merrifield
x86/platform/intel_mid_pci: Rework IRQ0 workaround
x86, thermal: Clean up and fix CPU model detection for intel_soc_dts_thermal
x86, mmc: Use Intel family name macros for mmc driver
x86/intel_telemetry: Use Intel family name macros for telemetry driver
x86/acpi/lss: Use Intel family name macros for the acpi_lpss driver
x86/cpufreq: Use Intel family name macros for the intel_pstate cpufreq driver
x86/platform: Use new Intel model number macros
x86/intel_idle: Use Intel family macros for intel_idle
...
This reverts commit 4ac0d5f245e1 ("mmc: sdhci-of-arasan: Always power
the PHY off/on when clock changes"), resolving conflicts with other
patches that have come after. It appears that on some boards / with
some eMMC devices that the patch is causing problems.
Presumably turning the phy off and on again at the wrong time while
initially setting up the card is confusing the card, the host, or the
PHY. We have lots of power cycles while initially setting up the card
because the main sdhci driver often turns off the clock by clearing
SDHCI_CLOCK_CARD_EN and then calls host->ops->set_clock() to set the
clock again. With all of those, we ended up with lots of power cycles.
Presumably the arguments made in the original patch still hold. That
is, whenever the card clock is turned off and on again (or changed) we
really should wait for the DLL to lock again. However, perhaps it's
really not that critical for the lower speeds.
It's possible that the right answer here is:
* Whenever set_clock() is called we should double-check that the DLL is
locked.
* Whenever set_clock() is called and we're actually changing clocks we
should do a power cycle around that.
* When we're doing a power cycle just because the clock changed, we
probably shouldn't do quite as many things (maybe don't need to
recalibarate, etc).
Unfortunately the interaction between SDHCI and the PHY is extremely
limited because of the limited PHY API. The PHY does have a reference
to the card clock and could theoretically register for notifications,
except that our clock is query only (it uses CLK_GET_RATE_NOCACHE) and
so can't really be notified about updates. I believe we would need a
major redesign of clock handling in SDHCI core to do better than that,
or we would need to make our one fake notifications. :(
Let's hope that we can eventually get more information from Arasan on
how all this should be handled before doing tons more work. Until then,
let's get back to a known working state. Note that the rest of the
patches in the 150 MHz series should still work fine even without this
one.
Signed-off-by: Douglas Anderson <dianders@chromium.org>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Enabling support for ultra high speed mode cards requires some
voltage switching and interaction with the PMIC via a special
power IRQ. Add support for this.
Signed-off-by: Georgi Djakov <georgi.djakov@linaro.org>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
To allow UHS mode to work properly, we need to implement a Qualcomm
specific set_uhs_signaling() callback function. This function differs
from the sdhci_set_uhs_signaling() in that we need check the clock
rate and enable UHS timing only if the frequency is above 100MHz.
This patch resolves the mmc_select_hs200 timeouts noticed after merging
commit a5c1f3e55c99 ("mmc: mmc: do not use CMD13 to get status after
speed mode switch")
mmc0: mmc_select_hs200 failed, error -110
mmc0: error -110 whilst initialising MMC card
mmc0: Reset 0x1 never completed.
sdhci: =========== REGISTER DUMP (mmc0)===========
sdhci: Sys addr: 0x00000000 | Version: 0x00002e02
sdhci: Blk size: 0x00004000 | Blk cnt: 0x00000000
sdhci: Argument: 0x00000000 | Trn mode: 0x00000000
sdhci: Present: 0x01f80000 | Host ctl: 0x00000000
sdhci: Power: 0x00000000 | Blk gap: 0x00000000
sdhci: Wake-up: 0x00000000 | Clock: 0x00000003
sdhci: Timeout: 0x00000000 | Int stat: 0x00000000
sdhci: Int enab: 0x00000000 | Sig enab: 0x00000000
sdhci: AC12 err: 0x00000000 | Slot int: 0x00000000
sdhci: Caps: 0x322dc8b2 | Caps_1: 0x00008007
sdhci: Cmd: 0x00000000 | Max curr: 0x00000000
sdhci: Host ctl2: 0x00000000
sdhci: ADMA Err: 0x00000000 | ADMA Ptr: 0x0000000000000000
sdhci: ===========================================
Fixes: a5c1f3e55c99 ("mmc: mmc: do not use CMD13 to get status after...")
Signed-off-by: Ritesh Harjani <riteshh@codeaurora.org>
Signed-off-by: Georgi Djakov <georgi.djakov@linaro.org>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The controller does not clear the "reset bit" when it is reset without
a card in the slot. Because of this, the following error message is seen
while booting with no plugged SD card.
mmc1: Reset 0x1 never completed.
Add the SDHCI_QUIRK_NO_CARD_NO_RESET quirk to avoid this.
Signed-off-by: Ivan T. Ivanov <ivan.ivanov@linaro.org>
Signed-off-by: Georgi Djakov <georgi.djakov@linaro.org>
Tested-by: Bjorn Andersson <bjorn.andersson@linaro.org>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
To support UHS modes for Tegra an external regulator must be present
to adjust the IO voltage accordingly. Even if the regulator is not
present but the host supports the UHS modes and the device supports the
UHS modes, then we will attempt to switch to a high-speed mode. Without
an external regulator, Tegra will fail to switch to the high-speed
mode.
It has been found that with some SD cards, that once it has been switch
to operate at a high-speed mode, all subsequent commands issues to the
card will fail and so it will not be possible to switch back to a non
high-speed mode and so the SD card initialisation will fail.
The SDHCI core does not require that the host have an external regulator
when switching to UHS modes and therefore, the Tegra SDHCI host
controller should only advertise the UHS modes as being supported if the
regulator for the IO voltage is present. Fortunately, Tegra has a vendor
specific register which can be used to control which modes are
advertised via the SDHCI_CAPABILITIES register. Hence, if there is no IO
voltage regulator available for the Tegra SDHCI host, then don't
advertise the UHS modes.
Note that if the regulator is not available, we also don't advertise that
the SDHCI is compatible with v3.0 of the SDHCI specification because
this will read the SDHCI_CAPABILITIES_1 register which will enable other
UHS modes.
This fixes commit 7ad2ed1dfc ("mmc: tegra: enable UHS-I modes") which
enables UHS mode without checking if the board can support them.
Fixes: 7ad2ed1dfc ("mmc: tegra: enable UHS-I modes")
Signed-off-by: Jon Hunter <jonathanh@nvidia.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The capabilities of the SDHCI host controller are read early during the
SDHCI host initialisation in sdhci_setup_host() and before any
regulators for the host have been requested. This means that if the host
supports some high-speed modes (according to its capabilities register),
but the board cannot because the appropriate voltage regulator is not
available, then the host cannot easily override the capabilities that
are supported.
To allow a SDHCI host controller to determine if it can support UHS high
speed modes via the presence of the MMC regulators, request the
regulators before reading the capabilities of the host controller. This
will allow the SDHCI host to use the 'reset' callback to take the
appropriate action (set flags, configure registers, etc) before the
capabilities register(s) are read.
Please note that some SDHCI hosts, such as the Tegra SDHCI host, has
the ability to mask bits in the capabilities register to prevent
certain capabilities from being advertised.
Signed-off-by: Jon Hunter <jonathanh@nvidia.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Everywhere else in the code MRFLD abbreviation is used for Intel Merrifield. Do
the same for sdhci-pci.
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The tuning bits like FBCLK_SEL, SMP_CLK_SEL and DLY_CELL which affects
timing may have already been set by ROM if booting from SD3.0 mode like
SDR104. Let's clear it first during driver probe before doing the new
card enumeration to avoid working on the wrong timing.
Note that tuning bits are dynamical settings which may need to be kept
during MMC_PM_KEEP_POWER suspend, so we did not put them into hwinit
function.
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
sdhci_esdhc_imx_hwinit() includes all basic hw intialization.
Calling it after resume to re-initialize hw in case its state
is already lost in low power mode.
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Move tuning static configuration into basic hwinit function.
Tuning configuration may also be lost in low power mode, so
need restore in hwinit().
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Move all hw related static initializations into a separate function
which helps concentrate the hw related initialization code.
And that function could also be called by other places later as a
basic hw state restore.
e.g. suspend/resume where the hw state is possible to lost due to
low power mode.
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
When enable DDR, the clock factor definition is changed.
e.g. original 200Mhz will become 100Mhz once MIX_CTRL_DDREN bit is set
So we need to update the clock setting then the strobe dll can lock
the correct clock rate.
Additionally we also need disable the clock before locking strobe dll.
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Indicating hw auto retuning support for mx6qdl in the fake caps_1
register and enable auto retuning in post_tuning process after
tuning completes.
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Enable HW auto retuning when set SDHCI_CTRL_EXEC_TUNING and clear it
when clear SDHCI_CTRL_TUNED_CLK.
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
If HW supports SDHCI_TUNING_MODE_3 which is auto retuning, we won't
retune during runtime suspend and resume, instead we use Re-tuning
Request signaled via SDHCI_INT_RETUNE interrupt to do retuning and
hw auto retuning during data transfer to guarantee the signal sample
window correction.
This can avoid a mass of repeatedly retuning during small file system
data access and improve the performance.
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The delay cells of some SoCs may have less delay per one cell,
for such SoCs, user could set the start delay cell point to bypass
the first a few meaningless tuning commands.
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Disable DLL delay line settings explicitly during driver initialization
in case ROM/uBoot had set an invalid delay.
e.g. MX6DL ROM has set the default delay line(DLLCTRL) to 0x1000021,
the uSDHC clock timing will become marginal when works on DDR mode
due to default delay and will possibly see CRC errors in case the board
is not perfectly designed on the eMMC chip layout.
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Currently, we config the watermark_level register only in probe.
This will cause the mmc write operation timeout issue after system
resume back in LPSR mode. Because in LPSR mode, after system resume
back, the watermark_level register(0x44) changes to 0x08000880, which
set the write watermark level as 0, and set the read watermark level
as 128. This value is incorrect.
This patch restores the setting of watermark level register after
system resume back.
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
It will be used for platform specific suspend/resume state save/restore
work for some low power mode like Mega/Fast or LPSR mode.
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The driver has already implemented the private .set_timeout()
callback for common SDHCI code to do correct timeout value setting,
it does not need call sdhci_calc_timeout(), so this quirk actually
is not working. Remove it now.
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Switch to use the more robust common mmc_regulator_set_vqmmc()
function in MMC core which set the target voltage as close as
possible to target voltage.
We did not re-factor the whole sdhci_start_signal_voltage_switch()
cause we want to keep the original signal switch order between host
and card to avoid potential break.
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This makes the error handling much more simpler than open-coding everything
and in addition makes the probe function smaller an tidier.
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In dw_mmc.c, it's enabled by default.
It doesn't need to set MMC_CAP_ERASE in rockchip anymore.
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Acked-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This flag needs to use the trim/discard/erase commands.
dwmmc controller enables this flag by default.
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The capabilities in iproc platform data are magic numbers. So
replace them with the proper capability defines to make it
readable.
Signed-off-by: Stefan Wahren <stefan.wahren@i2se.com>
Acked-by: Scott Branden <scott.branden@broadcom.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This patch adds the missing define for the suspend/resume
capability (according to SD Host Controller spec).
Signed-off-by: Stefan Wahren <stefan.wahren@i2se.com>
Acked-by: Scott Branden <scott.branden@broadcom.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The driver registered for CPU frequency transitions to recalculate its
clock when ARM clock frequency changes (ratio between frequencies of
ARM's parent clock (fclk) and clock for peripherals remains fixed).
This is needed only on S3C24xx platform when cpufreq driver is enabled
so limit the ifdef to respective cpufreq Kconfig.
Suggested-by: Marek Szyprowski <m.szyprowski@samsung.com>
Signed-off-by: Krzysztof Kozlowski <k.kozlowski@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
sdhci_send_command() starts a timer to catch cases where the host
controller fails. The timer is normally deleted when the request completes,
but in the case of sdhci_execute_tuning() the request is handled
differently and the timer is left running. This goes unnoticed because
tuning is done before another command so the timer gets reset then.
That should not be relied upon, so make sdhci_execute_tuning() delete the
timer.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The STOP command is sent in error conditions, even when the command is
not finished. Avoid triggering the warning for that in sdhci_send_command()
by setting host->cmd to NULL first.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to support commands during data transfer, it will be possible to
need to reset the command circuit while the data circuit is in use, and
vice versa. It is now easy to determine whether the command or data circuit
is in use, and so just skip the corresponding reset if it is.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Factor out sdhci_auto_cmd12() so that there is a single place that controls
whether auto-CMD12 is used.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to support commands during data transfer, there will have to be up
to two active requests (mrqs) at a time, instead of just one. That means
recording which request is finished. Doing that obsoletes host->mrq which
is therefore removed.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to support commands during data transfer, there will have to be up
to two active requests (mrqs) at a time, instead of just one. Provide two
timers instead of just one. One of the timers is for requests that do not
use the data lines, and the other one is for requests that do.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Factor out sdhci_data_line_cmd() to improve readability and because it is
used in multiple places.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to support commands during data transfer, there will have to be up
to two active requests (mrqs) at a time, instead of just one. That means
ensuring that all requests get errored out in the cases of card or driver
removal.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Several pointers are used to identify when interrupts are expected. Namely,
host->cmd, host->data_cmd and host->data. Ensure those are cleared when
a request finishes. That tidies the case when a request is errored out
before normal processing has completed, ensuring any interrupts that occur
subsequently are not acted upon.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
SDHCI recovers from errors by resetting the cmd and data circuits. Until
that is done, there very well might be more interrupts, so ignore them in
that case.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Factor out sdhci_needs_reset() so it can be reused.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to support commands during data transfer, there will have to be up
to two active requests (mrqs) at a time, instead of just one. That means
the driver must identify which one to finish. Prepare for that by factoring
out sdhci_finish_mrq().
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to support commands during data transfer, it will be possible
that host->data is not NULL when preparing a new request. Move a warning
that assumes otherwise.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to support commands during data transfer, there will have to be up
to two active requests (mrqs) at a time, instead of just one. That means
host->mrq will not be able to be used.
In several places, host->mrq is used when instead the mrq can be determined
from the cmd or data pointers. Reduce the use of host->mrq by doing that.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Now that there is host->data_cmd to record the command for which a data
interrupt is expected, it is possible to determine whether a command with
busy signaling has completed without an extra flag. So host->busy_handle
is not needed. Remove it.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to support commands during data transfer, there must be a
distinction between the command that is using the command line (and
for which a command interrupt is expected) and the command that is
using the data lines (for which a data interrupt is expected).
There is host->cmd for the command line, but there is only host->data
for the data lines, which is a different structure, does not represent
the command in use, and is anyway NULL in the case of commands that use
the data lines for busy signalling instead of data transfer.
Introduce host->data_cmd to record what command is using the data lines,
and use that instead of host->cmd when referring to the data command.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
sdhci_finish_command() is going to set host->cmd to NULL. Simplify the
code by using a local variable to hold host->cmd and set host->cmd to
NULL at the start.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
BUG is never the right thing for SDHCI to do. Get rid of BUG_ON in cases it
will oops anyway if the pointer is NULL, or if the condition is logically
impossible.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to support commands during data transfer, command and data
handling needs to be untangled.
That means sdhci_finish_cmd() must not be called from the data IRQ
handler. It is being called because of busy signal handling, which
is treating the command as not finished until the busy signal is
released.
Instead, move busy signal handling from sdhci_cmd_irq() into
sdhci_finish_cmd(). Then the data IRQ handler does not need to call
sdhci_finish_cmd() and can instead finish the request.
What this means in practice for a command with busy signaling, is that
the command response is read from the host controller when the command
complete interrupt is received, thus freeing up the command circuit for
other commands.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
At the successful conclusion of sdhci_pci_probe(), if runtime pm was
allowed, the device would be runtime suspended. That wastes a lot of time
during initialization. Instead leave the device active until the mmc core
scans for a card.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Add sdhci_read_caps() and __sdhci_read_caps() to make it easier for drivers
to fix the version and capabilities registers.
Pedantically, the SDHCI specification states that the capabilities
registers are valid when the host controller resets the Software Reset For
All bit. That requirement has always been satisfied by performing a reset
at the start of initialization, and consequently that is now part of the
new functions.
Although the SDHCI_QUIRK_MISSING_CAPS quirk has not yet been removed,
drivers that want to provide their own caps can now use these functions
instead of that quirk.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In preparation for adding a function to read the capability registers.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Signal voltage support is not a quirk, it is a capability. According to the
SDHCI specification, support for 1.8V signaling is determined by the
presence of one of the capability bits SDHCI_SUPPORT_SDR50,
SDHCI_SUPPORT_SDR104, or SDHCI_SUPPORT_DDR50. This is complicated by also
supporting eMMC which has 1.8V modes and 1.2V modes. It would be possible
to use the transfer mode to determine signal voltage support, except for
eMMC DDR52 mode which uses the same capability (MMC_CAP_1_8V_DDR) for 1.8V
signaling and 3V signaling.
In addition, the mmc core will fail over from one signaling voltage to the
next (refer mmc_power_up()) which means SDHCI really needs to validate
which voltages are actually supported.
Introduce SDHCI flags for signal voltage support and set them based on the
supported transfer modes. In general, drivers should prefer to set the
supported transfer modes correctly rather than change the signal voltage
capability, except in the case where 3V DDR52 is supported but 1.8V is
not.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Split sdhci-add_host() in order to further our objective to make
sdhci into a library.
The split divides code that sets up mmc and sdhci parameters, from
code that actually activates things - such as tasklet initialization,
requesting the irq, and adding (and starting) the host.
This gives drivers an opportunity to change various settings before
committing to start the host.
Drivers can continue to call sdhci_add_host() but drivers that want
to take advantage of the split instead call sdhci_setup_host() followed
by __sdhci_add_host().
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Drivers must be able to provide their own implementations for mmc host
operations. Consequently, SDHCI should call those not the default
implementations. Do that by calling indirectly through the mmc host ops
function pointers.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
in our host design, rise edge latching is more stable than fall edge
latching. so that if rise edge has enough margin, no need scan fall edge.
Signed-off-by: Chaotian Jing <chaotian.jing@mediatek.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
we did not deal with the read data of CMD21/CMD19 if there is
response CRC error of CMD21/CMD19, in this case, eMMC/SD may
still in send-data state. therefore, all of next commands cannot
get response as device is not in transfer state.
for resolving this issue, still need deal with the data receive
to make device back to transfer state.
Signed-off-by: Chaotian Jing <chaotian.jing@mediatek.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
the tune result of hs200 mode at 200Mhz is not suitable for 50Mhz,
mmc_select_hs400() will set clock frequency to 50Mhz, use defalut
tune setting for 50Mhz to avoid CRC error.
Signed-off-by: Chaotian Jing <chaotian.jing@mediatek.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
for hs400 mode, should only tune DS delay, should not
tune PAD_TUNE for data path.
if eMMC will run at hs400 mode, do not tune data while
call ops->execute_tuning().
Signed-off-by: Chaotian Jing <chaotian.jing@mediatek.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
DATA_OVER(the same for RI/TI of IDMAC) interrupt may come
up together with data error interrupts. If so, the interrupt
routine set EVENT_DATA_ERR to the pending_events and schedule
the tasklet but we may still fallback to the IDMAC interrupt
case as the tasklet may come up a little late, namely right
after the IDMAC interrupt checking. This will casue dw_mmc
unmap sg twice. We can easily see it with CONFIG_DMA_API_DEBUG
enabled.
WARNING: CPU: 0 PID: 0 at lib/dma-debug.c:1096 check_unmap+0x7bc/0xb38
dwmmc_exynos 12200000.mmc: DMA-API: device driver tries to free DMA memory it
has not allocated [device address=0x000000006d9d2200]
[size=128 bytes]
Modules linked in:
CPU: 0 PID: 0 Comm: swapper/0 Not tainted 4.7.0-rc4 #26
Hardware name: SAMSUNG EXYNOS (Flattened Device Tree)
[<c0112b4c>] (unwind_backtrace) from [<c010d888>] (show_stack+0x20/0x24)
[<c010d888>] (show_stack) from [<c03fab0c>] (dump_stack+0x80/0x94)
[<c03fab0c>] (dump_stack) from [<c0123548>] (__warn+0xf8/0x110)
[<c0123548>] (__warn) from [<c01235a8>] (warn_slowpath_fmt+0x48/0x50)
[<c01235a8>] (warn_slowpath_fmt) from [<c042ac90>] (check_unmap+0x7bc/0xb38)
[<c042ac90>] (check_unmap) from [<c042b25c>] (debug_dma_unmap_sg+0x118/0x148)
[<c042b25c>] (debug_dma_unmap_sg) from [<c077512c>] (dw_mci_dma_cleanup+0x7c/0xb8)
[<c077512c>] (dw_mci_dma_cleanup) from [<c0773f24>] (dw_mci_stop_dma+0x40/0x50)
[<c0773f24>] (dw_mci_stop_dma) from [<c0777d04>] (dw_mci_tasklet_func+0x130/0x3b4)
[<c0777d04>] (dw_mci_tasklet_func) from [<c0129760>] (tasklet_action+0xb4/0x150)
..[snip]..
---[ end trace 256f83eed365daf0 ]---
Reported-by: Seung-Woo Kim <sw0312.kim@samsung.com>
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Since v2.80a, dwmmc controller introduced the card write threshold for
HS400 mode. So CardThrCtl can be supported during write operation, not
only read operation.
(Note: Only use the write threshold when mode is HS400.)
To use more compatible, removed "_rd_" from function name.
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Remove the quirks flag. (DW_MCI_QUIRK_BROKEN_DTO)
For removing this, enabled the dto_timer by defaults.
It doesn't see any I/O performance degression.
In future, dwmmc controller should not use the quirks flag.
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
"host->cur_slot" should be assigned to start the request.
So it can be the NULL pointer. This patch fixed this error.
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This patch removes following UBSAN warnings in dw_mci_setup_bus().
UBSAN: Undefined behaviour in drivers/mmc/host/dw_mmc.c:1102:14
shift exponent 250 is too large for 32-bit type 'unsigned int'
Call trace:
[<ffffff90080908a8>] dump_backtrace+0x0/0x380
[<ffffff9008090c3c>] show_stack+0x14/0x20
[<ffffff90087457b8>] dump_stack+0xe0/0x120
[<ffffff90087b1360>] ubsan_epilogue+0x18/0x68
[<ffffff90087b1a94>] __ubsan_handle_shift_out_of_bounds+0x18c/0x1bc
[<ffffff9008d89cb8>] dw_mci_setup_bus+0x3a0/0x438
[...]
UBSAN: Undefined behaviour in drivers/mmc/host/dw_mmc.c:1132:27
shift exponent 250 is too large for 32-bit type 'unsigned int'
Call trace:
[<ffffff90080908a8>] dump_backtrace+0x0/0x380
[<ffffff9008090c3c>] show_stack+0x14/0x20
[<ffffff90087457b8>] dump_stack+0xe0/0x120
[<ffffff90087b1360>] ubsan_epilogue+0x18/0x68
[<ffffff90087b1a94>] __ubsan_handle_shift_out_of_bounds+0x18c/0x1bc
[<ffffff9008d89c9c>] dw_mci_setup_bus+0x384/0x438
[...]
The warnings are caused because of bit shift which is used to
filter spamming message for CONFIG_MMC_CLKGATE, but the config is
already removed. So this patch just removes the shift.
Signed-off-by: Seung-Woo Kim <sw0312.kim@samsung.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
According to the DesignWare state machine description, after we get a
"response error" or "response CRC error" we move into data transfer
mode. That means that we don't necessarily need to special case
trying to deal with the failure right away. We can wait until we are
notified that the data transfer is complete (with or without errors)
and then we can deal with the failure.
It may sound strange to defer dealing with a command that we know will
fail anyway, but this appears to fix a bug. During tuning (CMD19) on
a specific card on an rk3288-based system, we found that we could get
a "response CRC error". Sending the stop command after the "response
CRC error" would then throw the system into a confused state causing
all future tuning phases to report failure.
When in the confused state, the controller would show these (hex codes
are interrupt status register):
CMD ERR: 0x00000046 (cmd=19)
CMD ERR: 0x0000004e (cmd=12)
DATA ERR: 0x00000208
DATA ERR: 0x0000020c
CMD ERR: 0x00000104 (cmd=19)
CMD ERR: 0x00000104 (cmd=12)
DATA ERR: 0x00000208
DATA ERR: 0x0000020c
...
...
It is inherently difficult to deal with the complexity of trying to
correctly send a stop command while a data transfer is taking place
since you need to deal with different corner cases caused by the fact
that the data transfer could complete (with errors or without errors)
during various places in sending the stop command (dw_mci_stop_dma,
send_stop_abort, etc)
Instead of adding a bunch of extra complexity to deal with this, it
seems much simpler to just use the more straightforward (and less
error-prone) path of letting the data transfer finish. There
shouldn't be any huge benefit to sending the stop command slightly
earlier, anyway.
Signed-off-by: Doug Anderson <dianders@chromium.org>
Signed-off-by: Enric Balletbo i Serra <enric.balletbo@collabora.com>
Cc: Alim Akhtar <alim.akhtar@gmail.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The IDMAC_SET_BUFFER1_SIZE() macro modifies des1, but does
not check if the value being passed is big or little endian
desptire the des1 field being marked as __le32.
Fix the issue by ensuring the values are changed from the
cpu endian to the descriptor endian by using cpu_to_le32.
Spotted whilst doing big endian conversion work on Exynos,
and stops the mmc worker thread from stalling.
Signed-off-by: Ben Dooks <ben.dooks@codethink.co.uk>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
Tested-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The dw_mmc driver enables HLE errors as part of DW_MCI_ERROR_FLAGS but
nothing in the interrupt handler actually handles them and ACKs them.
That means that if we ever get an HLE error we'll just keep getting
interrupts and we'll wedge things.
We really don't expect HLE errors but if we ever get them we shouldn't
silently ignore them.
Note that I have seen HLE errors while constantly ejecting and
inserting cards (ejecting while inserting, etc).
Signed-off-by: Doug Anderson <dianders@chromium.org>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Enables RPMB support for the on-board eMMC of the HiKey board as well
as for eMMC modules connected to the microSD slot.
Signed-off-by: Jerome Forissier <jerome.forissier@linaro.org>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The main reason to add this check is to avoid unnecessary
mmc_request like the on-going cmd and the corresponding sbc
if the card is removed. Although we have already checked this in
dw_mci_handle_cd for runtime usage of sd card and dw_mci_init_slot
for noremovable devices, but there is a timing gap before it really
calls dw_mci_get_cd as mmc_detect_change needs some delay here.
Another gain here is that we could save some checkings of card status
after sd card been removed.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
dw_mci_get_cd have already dealt with these for
both of internal card-detect and gpio card-detect.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The current value means an mdelay(1) may execute up to 10000000 times,
which translates to around ~2.8 hours. This is probably not what the
orignal author had in mind. Let's instead use 10s, which is the same value
sh_mmcif is using for other timeouts.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The sh_mmcif driver is already using a 10s request timeout. Let's also
inform the mmc core about this value, as there are situations when it
needs to know about it.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The sh_mmcif explicity checks for certain commands to decide when to
enable HW busy detection. Instead, it should only check the response type
as it tells if busy detection is needed.
In this way, the mmc core also gets full control whether it thinks busy
detection should be done or not. In some specific scenarios, like for
ERASE and STOP commands it may decide to fall back to use a CMD13 to poll
the card status instead.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Enable the capabilities which tells the mmc core to prevent sending SD and
SDIO commands during card initialization. In this way, we can also remove
the validation of non-supported commands in the ->request() callback.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
trivial fix to spelling mistake in dev_err message
Signed-off-by: Colin Ian King <colin.king@canonical.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
sdhci_dumpregs is used to dump registers when error happens. Thus it should
use pr_err instead of pr_debug to show more information about the hardware.
Signed-off-by: Chuanxiao Dong <chuanxiao.dong@intel.com>
[Fix whitespace and checkpatch warnings]
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In linux/mmc/host.h, mmc_card_is_removable() is already defined.
It should be maintainted more easier than now.
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Some SD/eMMC PHYs (like the PHY from Arasan that is designed to work
with arasan,sdhci-5.1) need to know the card clock in order to function
properly. Let's add the ability to expose this clock. Any PHY that
needs to know the clock rate can add a reference and query the clock
rate.
At the moment we register a CLK_GET_RATE_NOCACHE clock that simply
allows querying the clock. This allows us to be less intrusive with
regards to the main SDHCI driver, which has complex logic for adjusting
the SD clock. Right now we always fully power cycle the PHY when the
clock changes and that gives the PHY a good chance to query our clock.
Signed-off-by: Douglas Anderson <dianders@chromium.org>
Reviewed-by: Heiko Stuebner <heiko@sntech.de>
Tested-by: Heiko Stuebner <heiko@sntech.de>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In the the earlier change in this series ("Documentation: mmc:
sdhci-of-arasan: Add soc-ctl-syscon for corecfg regs") we can see the
mechansim for specifying a syscon to properly set corecfg registers in
sdhci-of-arasan. Now let's use this mechanism to properly set
corecfg_baseclkfreq on rk3399.
>From [1] the corecfg_baseclkfreq is supposed to be set to:
Base Clock Frequency for SD Clock.
This is the frequency of the xin_clk.
This is a relatively easy thing to do. Note that we assume that xin_clk
is not dynamic and we can check the clock at probe time. If any real
devices have a dynamic xin_clk future patches could register for
notifiers for the clock.
At the moment, setting corecfg_baseclkfreq is only supported for rk3399
since we need a specific map for each implementation. The code is
written in a generic way that should make this easy to extend to other
SoCs. Note that a specific compatible string for rk3399 is already in
use and so we add that to the table to match rk3399.
[1]: https://arasan.com/wp-content/media/eMMC-5-1-Total-Solution_Rev-1-3.pdf
Signed-off-by: Douglas Anderson <dianders@chromium.org>
Reviewed-by: Heiko Stuebner <heiko@sntech.de>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
Tested-by: Heiko Stuebner <heiko@sntech.de>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In commit 802ac39a55 ("mmc: sdhci-of-arasan: fix set_clock when a phy
is supported") we added code to power the PHY off and on whenever the
clock was changed but we avoided doing the power cycle code when the
clock was low speed. Let's now do it always.
Although there may be other reasons for power cycling the PHY when the
clock changes, one of the main reasons is that we need to give the DLL a
chance to re-lock with the new clock.
One of the things that the DLL is for is tuning the Receive Clock in
HS200 mode and STRB in HS400 mode. Thus it is clear that we should make
sure we power cycle the PHY (and wait for the DLL to lock) when we know
we'll be in one of these two speed modes. That's what the original code
did, though it used the clock rate rather than the speed mode. However,
even in speed modes other than HS200,/HS400 the DLL is used for
something since it can be clearly observed that the PHY doesn't function
properly if you leave the DLL off.
Although it appears less important to power cycle the PHY and wait for
the DLL to lock when not in HS200/HS400 modes (no bugs were reported),
it still seems wise to let the locking always happen nevertheless.
Note: as part of this, we make sure that we never try to turn the PHY on
when the clock is off (when the clock rate is 0). The PHY cannot work
when the clock is off since its DLL can't lock.
This change requires ("phy: rockchip-emmc: Increase lock time
allowance") and will cause problems if picked without that change.
Signed-off-by: Douglas Anderson <dianders@chromium.org>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
Tested-by: Heiko Stuebner <heiko@sntech.de>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Add SDHCI driver for Broadcom BRCMSTB SoCs.
This driver works with all ARM based SoCs and the 7425, 7429
and 7435 MIPS based SoCs.
The driver disables all UHS speed modes by default and relies
on the Device Tree node properties to enable these modes for
SoC/Board combinations that support them.
Signed-off-by: Al Cooper <alcooperx@gmail.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The sdhci-bcm2835 is no more needed since it has been replaced
by sdhci-iproc.
Signed-off-by: Stefan Wahren <stefan.wahren@i2se.com>
Acked-by: Eric Anholt <eric@anholt.net>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
host->card_busy() was introduced for SD voltage switching which checks all
4 data lines.
Increasingly, host->card_busy is being used to poll the the busy signal
which is only data line 0 (DAT[0]).
The current logic in sdhci_card_busy() does not work in that case because
it returns false if any of the data lines is high. It also ignores
possibilities:
- data lines 1-3 are not connected and could show at any level
- data lines 1-2 can be used by SDIO for other purposes
According to the SD specification, it is OK to check any of the data lines
for voltage switching, so change to use DAT[0] only.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Sparse complains about the implicit cast. Making it explicit is indeed
better coding style.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Currently sdhci-arasan 5.1 can support enhanced strobe function,
and we now limit it just for "arasan,sdhci-5.1". Add
mmc-hs400-enhanced-strobe in DT to enable the function if we're
sure our controller can support it.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Reviewed-by: Doug Anderson <dianders@chromium.org>
Tested-by: Doug Anderson <dianders@chromium.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Activating wakeup event is not enough to get a wakeup signal. The
corresponding events have to be enabled in the Interrupt Status Enable
Register too. It follows the specification and is needed at least by
sdhci-of-at91.
Signed-off-by: Ludovic Desroches <ludovic.desroches@atmel.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Since commit 7ce45e9506 ("mmc: sdhci: SD tuning is broken for some
controllers") sdhci_execute_tuning() no longer includes a timeout in its
loop counter(s) so remove portion of the comment regarding this.
Signed-off-by: Simon Horman <horms+renesas@verge.net.au>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Replace hardcoded values with meaningful names and document what we
know.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Reviewed-by: Simon Horman <horms+renesas@verge.net.au>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
As reported by Dan in his report in [1], there is a potential NULL
pointer derefence if these conditions are met :
- there is no platform_data provided, ie. host->pdata = NULL
Fix this by only using the platform data ro_invert when a gpio for
read-only is provided by the platform data.
This doesn't appear yet as every pxa board provides a platform_data, and
calls pxa_set_mci_info() with a non NULL pointer.
[1] [bug report] mmc: pxamci: fix card detect with slot-gpio API.
The commit fd546ee6a7 ("mmc: pxamci: fix card detect with slot-gpio
API") from Sep 26, 2015, leads to the following static checker warning:
drivers/mmc/host/pxamci.c:809 pxamci_probe()
warn: variable dereferenced before check 'host->pdata' (see line 798)
Fixes: fd546ee6a7 ("mmc: pxamci: fix card detect with slot-gpio API")
Reported-by: Dan Carpenter <dan.carpenter@oracle.com>
Signed-off-by: Robert Jarzmik <robert.jarzmik@free.fr>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
We now have implicit batching in the timer wheel. The slack API is no longer
used, so remove it.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Alan Stern <stern@rowland.harvard.edu>
Cc: Andrew F. Davis <afd@ti.com>
Cc: Arjan van de Ven <arjan@infradead.org>
Cc: Chris Mason <clm@fb.com>
Cc: David S. Miller <davem@davemloft.net>
Cc: David Woodhouse <dwmw2@infradead.org>
Cc: Dmitry Eremin-Solenikov <dbaryshkov@gmail.com>
Cc: Eric Dumazet <edumazet@google.com>
Cc: Frederic Weisbecker <fweisbec@gmail.com>
Cc: George Spelvin <linux@sciencehorizons.net>
Cc: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Cc: Jaehoon Chung <jh80.chung@samsung.com>
Cc: Jens Axboe <axboe@kernel.dk>
Cc: John Stultz <john.stultz@linaro.org>
Cc: Josh Triplett <josh@joshtriplett.org>
Cc: Len Brown <lenb@kernel.org>
Cc: Linus Torvalds <torvalds@linux-foundation.org>
Cc: Mathias Nyman <mathias.nyman@intel.com>
Cc: Pali Rohár <pali.rohar@gmail.com>
Cc: Paul E. McKenney <paulmck@linux.vnet.ibm.com>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: Rik van Riel <riel@redhat.com>
Cc: Sebastian Reichel <sre@kernel.org>
Cc: Ulf Hansson <ulf.hansson@linaro.org>
Cc: linux-block@vger.kernel.org
Cc: linux-kernel@vger.kernel.org
Cc: linux-mmc@vger.kernel.org
Cc: linux-pm@vger.kernel.org
Cc: linux-usb@vger.kernel.org
Cc: netdev@vger.kernel.org
Cc: rt@linutronix.de
Link: http://lkml.kernel.org/r/20160704094342.189813118@linutronix.de
Signed-off-by: Ingo Molnar <mingo@kernel.org>
Now the the HS-DDR mode clock timings have been corrected, we can
re-enable these modes on the A80.
Signed-off-by: Chen-Yu Tsai <wens@csie.org>
Acked-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The MMC clock timings were incorrectly calculated, when the conversion
from delay value to delay phase was done.
The 50M DDR and 50M DDR 8bit timings are off, and make eMMC DDR
unusable. Unfortunately it seems different controllers on the same SoC
have different timings. The new settings are taken from mmc2, which is
commonly used with eMMC.
The settings for the slower timing modes seem to work despite being
wrong, so leave them be.
Signed-off-by: Chen-Yu Tsai <wens@csie.org>
Acked-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Most users of IS_ERR_VALUE() in the kernel are wrong, as they
pass an 'int' into a function that takes an 'unsigned long'
argument. This happens to work because the type is sign-extended
on 64-bit architectures before it gets converted into an
unsigned type.
However, anything that passes an 'unsigned short' or 'unsigned int'
argument into IS_ERR_VALUE() is guaranteed to be broken, as are
8-bit integers and types that are wider than 'unsigned long'.
Andrzej Hajda has already fixed a lot of the worst abusers that
were causing actual bugs, but it would be nice to prevent any
users that are not passing 'unsigned long' arguments.
This patch changes all users of IS_ERR_VALUE() that I could find
on 32-bit ARM randconfig builds and x86 allmodconfig. For the
moment, this doesn't change the definition of IS_ERR_VALUE()
because there are probably still architecture specific users
elsewhere.
Almost all the warnings I got are for files that are better off
using 'if (err)' or 'if (err < 0)'.
The only legitimate user I could find that we get a warning for
is the (32-bit only) freescale fman driver, so I did not remove
the IS_ERR_VALUE() there but changed the type to 'unsigned long'.
For 9pfs, I just worked around one user whose calling conventions
are so obscure that I did not dare change the behavior.
I was using this definition for testing:
#define IS_ERR_VALUE(x) ((unsigned long*)NULL == (typeof (x)*)NULL && \
unlikely((unsigned long long)(x) >= (unsigned long long)(typeof(x))-MAX_ERRNO))
which ends up making all 16-bit or wider types work correctly with
the most plausible interpretation of what IS_ERR_VALUE() was supposed
to return according to its users, but also causes a compile-time
warning for any users that do not pass an 'unsigned long' argument.
I suggested this approach earlier this year, but back then we ended
up deciding to just fix the users that are obviously broken. After
the initial warning that caused me to get involved in the discussion
(fs/gfs2/dir.c) showed up again in the mainline kernel, Linus
asked me to send the whole thing again.
[ Updated the 9p parts as per Al Viro - Linus ]
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Cc: Andrzej Hajda <a.hajda@samsung.com>
Cc: Andrew Morton <akpm@linux-foundation.org>
Link: https://lkml.org/lkml/2016/1/7/363
Link: https://lkml.org/lkml/2016/5/27/486
Acked-by: Srinivas Kandagatla <srinivas.kandagatla@linaro.org> # For nvmem part
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
The CMD19/CMD14 bus width test has been found to be unreliable in
some cases. It is not essential, so simply remove it.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Cc: stable@vger.kernel.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The CMD19/CMD14 bus width test has been found to be unreliable in
some cases. It is not essential, so simply remove it.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Cc: stable@vger.kernel.org
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Historically for Rockchip devices we've relied on the power-on
default (or perhaps the firmware setting) to get the correct drive
phase for dw_mmc devices. This worked OK for the most part, but:
* Relying on the setting just "being right" is a bit fragile.
* As soon as there is an instance where the power on default is wrong or
where the firmware didn't configure this properly then we'll get a
mysterious failure.
In commit 7a03fe6f48 ("clk: rockchip: reset init state before mmc card
initialization") we actually started setting this explicitly in the
kernel, but that commit wasn't quite right and also wasn't quite
enough. See <https://patchwork.kernel.org/patch/9085311/> for some
details.
Let's explicitly set this phase in dw_mmc.
The comments inside this patch try to explain the situation quite
throughly, but the high level overview of this is:
Before this patch on rk3288 devices tested (after revert of the clock
patch described above):
* eMMC: 180 degrees
* SDMMC/SDIO0/SDIO1: 90 degrees
After this patch:
* Use 90 degree phase offset usually.
* Use 180 degree phase offset for MMC_DDR52, SDR104, HS200.
That means we are _changing_ behavior for those devices in this way:
* If we have HS200 eMMC or DDR52 eMMC, we'll run ID mode at 90
degrees (vs 180) but otherwise have no change.
* For any non-HS200 / non-DDR52 eMMC devices we'll now _always_ run at
90 degrees (vs 180). It seems fairly unlikely that building modern
hardware is using an eMMC that isn't using DDR52 or HS200, of course.
* For SDR104 cards we'll now run with 180 degree phase offset (vs 90).
It's expected that 90 degree phase offset would have worked OK, but
this gives us extra margin.
I have tested this by inserting my collection of uSD cards (mostly UHS,
though a few not) into a veyron_minnie and confirmed that they still
seem to enumerate properly. For a subset of them I tried putting a
filesystem on them and also tried running mmc_test.
Fixes: 7a03fe6f48 ("clk: rockchip: reset init state before mmc card initialization")
Signed-off-by: Douglas Anderson <dianders@chromium.org>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
Tested-by: Heiko Stuebner <heiko@sntech.de>
Tested-by: Enric Balletbo i Serra <enric.balletbo@collabora.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
According to DesignWare TRM, BLKSIZ is 16bits.
Then it's correct that max_blk_size should be 0xFFFF, not 0x10000.
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Reviewed-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Some devices connected to the SDHCI controller may have separate enabling
lines that are controlled through GPIO. These devices need to be powered
on and enabled before probing. This is to ensure all devices connected can
be seen by the controller.
Note, for "stable" this patch depends on the following change:
commit 78a898d0e3 ("ACPI / PM: Export acpi_device_fix_up_power()")
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Reported-and-tested-by: Laszlo Fiat <laszlo.fiat@gmail.com>
Cc: <stable@vger.kernel.org> # 4.5+
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Reported-by: Laszlo Fiat <laszlo.fiat@gmail.com>
Bugzilla: https://bugzilla.kernel.org/show_bug.cgi?id=112571
Link: http://lkml.kernel.org/r/CA+7w51inLtQSr656bJvOjGG9oQWKYPXH+xxDPJKbeJ=CcrkS9Q@mail.gmail.com
- New cpufreq "schedutil" governor (making decisions based on CPU
utilization information provided by the scheduler and capable of
switching CPU frequencies right away if the underlying driver
supports that) and support for fast frequency switching in the
acpi-cpufreq driver (Rafael Wysocki).
- Consolidation of CPU frequency management on ARM platforms allowing
them to get rid of some platform-specific boilerplate code if they
are going to use the cpufreq-dt driver (Viresh Kumar, Finley Xiao,
Marc Gonzalez).
- Support for ACPI _PPC and CPU frequency limits in the intel_pstate
driver (Srinivas Pandruvada).
- Fixes and cleanups in the cpufreq core and generic governor code
(Rafael Wysocki, Sai Gurrappadi).
- intel_pstate driver optimizations and cleanups (Rafael Wysocki,
Philippe Longepe, Chen Yu, Joe Perches).
- cpufreq powernv driver fixes and cleanups (Akshay Adiga, Shilpasri
Bhat).
- cpufreq qoriq driver fixes and cleanups (Jia Hongtao).
- ACPI cpufreq driver cleanups (Viresh Kumar).
- Assorted cpufreq driver updates (Ashwin Chaugule, Geliang Tang,
Javier Martinez Canillas, Paul Gortmaker, Sudeep Holla).
- Assorted cpufreq fixes and cleanups (Joe Perches, Arnd Bergmann).
- Fixes and cleanups in the OPP (Operating Performance Points)
framework, mostly related to OPP sharing, and reorganization of
OF-dependent code in it (Viresh Kumar, Arnd Bergmann, Sudeep Holla).
- New "passive" governor for devfreq (for SoC subsystems that will
rely on someone else for the management of their power resources)
and consolidation of devfreq support for Exynos platforms, coding
style and typo fixes for devfreq (Chanwoo Choi, MyungJoo Ham).
- PM core fixes and cleanups, mostly to make it work better with the
generic power domains (genpd) framework, and updates for that
framework (Ulf Hansson, Thierry Reding, Colin Ian King).
- Intel Broxton support for the intel_idle driver (Len Brown).
- cpuidle core optimization and fix (Daniel Lezcano, Dave Gerlach).
- ARM cpuidle cleanups (Jisheng Zhang).
- Intel Kabylake support for the RAPL power capping driver (Jacob Pan).
- AVS (Adaptive Voltage Switching) rockchip-io driver update (Heiko
Stuebner).
- Updates for the cpupower tool (Arjun Sreedharan, Colin Ian King,
Mattia Dongili, Thomas Renninger).
/
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Merge tag 'pm-4.7-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/rafael/linux-pm
Pull power management updates from Rafael Wysocki:
"The majority of changes go into the cpufreq subsystem this time.
To me, quite obviously, the biggest ticket item is the new "schedutil"
governor. Interestingly enough, it's the first new cpufreq governor
since the beginning of the git era (except for some out-of-the-tree
ones).
There are two main differences between it and the existing governors.
First, it uses the information provided by the scheduler directly for
making its decisions, so it doesn't have to track anything by itself.
Second, it can invoke drivers (supporting that feature) to adjust CPU
performance right away without having to spawn work items to be
executed in process context or similar. Currently, the acpi-cpufreq
driver is the only one supporting that mode of operation, but then it
is used on a large number of systems.
The "schedutil" governor as included here is very simple and mostly
regarded as a foundation for future work on the integration of the
scheduler with CPU power management (in fact, there is work in
progress on top of it already). Nevertheless it works and the
preliminary results obtained with it are encouraging.
There also is some consolidation of CPU frequency management for ARM
platforms that can add their machine IDs the the new stub dt-platdev
driver now and that will take care of creating the requisite platform
device for cpufreq-dt, so it is not necessary to do that in platform
code any more. Several ARM platforms are switched over to using this
generic mechanism.
In addition to that, the intel_pstate driver is now going to respect
CPU frequency limits set by the platform firmware (or a BMC) and
provided via the ACPI _PPC object.
The devfreq subsystem is getting a new "passive" governor for SoCs
subsystems that will depend on somebody else to manage their voltage
rails and its support for Samsung Exynos SoCs is consolidated.
The rest is support for new hardware (Intel Broxton support in
intel_idle for one example), bug fixes, optimizations and cleanups in
a number of places.
Specifics:
- New cpufreq "schedutil" governor (making decisions based on CPU
utilization information provided by the scheduler and capable of
switching CPU frequencies right away if the underlying driver
supports that) and support for fast frequency switching in the
acpi-cpufreq driver (Rafael Wysocki)
- Consolidation of CPU frequency management on ARM platforms allowing
them to get rid of some platform-specific boilerplate code if they
are going to use the cpufreq-dt driver (Viresh Kumar, Finley Xiao,
Marc Gonzalez)
- Support for ACPI _PPC and CPU frequency limits in the intel_pstate
driver (Srinivas Pandruvada)
- Fixes and cleanups in the cpufreq core and generic governor code
(Rafael Wysocki, Sai Gurrappadi)
- intel_pstate driver optimizations and cleanups (Rafael Wysocki,
Philippe Longepe, Chen Yu, Joe Perches)
- cpufreq powernv driver fixes and cleanups (Akshay Adiga, Shilpasri
Bhat)
- cpufreq qoriq driver fixes and cleanups (Jia Hongtao)
- ACPI cpufreq driver cleanups (Viresh Kumar)
- Assorted cpufreq driver updates (Ashwin Chaugule, Geliang Tang,
Javier Martinez Canillas, Paul Gortmaker, Sudeep Holla)
- Assorted cpufreq fixes and cleanups (Joe Perches, Arnd Bergmann)
- Fixes and cleanups in the OPP (Operating Performance Points)
framework, mostly related to OPP sharing, and reorganization of
OF-dependent code in it (Viresh Kumar, Arnd Bergmann, Sudeep Holla)
- New "passive" governor for devfreq (for SoC subsystems that will
rely on someone else for the management of their power resources)
and consolidation of devfreq support for Exynos platforms, coding
style and typo fixes for devfreq (Chanwoo Choi, MyungJoo Ham)
- PM core fixes and cleanups, mostly to make it work better with the
generic power domains (genpd) framework, and updates for that
framework (Ulf Hansson, Thierry Reding, Colin Ian King)
- Intel Broxton support for the intel_idle driver (Len Brown)
- cpuidle core optimization and fix (Daniel Lezcano, Dave Gerlach)
- ARM cpuidle cleanups (Jisheng Zhang)
- Intel Kabylake support for the RAPL power capping driver (Jacob
Pan)
- AVS (Adaptive Voltage Switching) rockchip-io driver update (Heiko
Stuebner)
- Updates for the cpupower tool (Arjun Sreedharan, Colin Ian King,
Mattia Dongili, Thomas Renninger)"
* tag 'pm-4.7-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/rafael/linux-pm: (112 commits)
intel_pstate: Clean up get_target_pstate_use_performance()
intel_pstate: Use sample.core_avg_perf in get_avg_pstate()
intel_pstate: Clarify average performance computation
intel_pstate: Avoid unnecessary synchronize_sched() during initialization
cpufreq: schedutil: Make default depend on CONFIG_SMP
cpufreq: powernv: del_timer_sync when global and local pstate are equal
cpufreq: powernv: Move smp_call_function_any() out of irq safe block
intel_pstate: Clean up intel_pstate_get()
cpufreq: schedutil: Make it depend on CONFIG_SMP
cpufreq: governor: Fix handling of special cases in dbs_update()
PM / OPP: Move CONFIG_OF dependent code in a separate file
cpufreq: intel_pstate: Ignore _PPC processing under HWP
cpufreq: arm_big_little: use generic OPP functions for {init, free}_opp_table
PM / OPP: add non-OF versions of dev_pm_opp_{cpumask_, }remove_table
cpufreq: tango: Use generic platdev driver
PM / OPP: pass cpumask by reference
cpufreq: Fix GOV_LIMITS handling for the userspace governor
cpupower: fix potential memory leak
PM / devfreq: style/typo fixes
PM / devfreq: exynos: Add the detailed correlation for Exynos5422 bus
..
Tested on a Salvator-X board with a Spectec SDW-823 WLAN card.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
After commit d6463f170cf0 ("mmc: sdhci: Remove redundant runtime PM calls"),
some of original sdhci_do_xx() function wrappers becomes meaningless,
so remove them.
Signed-off-by: Dong Aisheng <aisheng.dong@nxp.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
commit 61b914eb81f8 ("mmc: sdhci-of-arasan: add phy support for
sdhci-of-arasan") introduce phy support for arasan. According to
the vendor's databook, we should make sure the phy is in poweroff
status before we configure the clk stuff. Otherwise it may cause
some IO sample timing issues from the test. And we don't need this
extra operation while running in low performance mode since phy
doesn't trigger sampling block.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
With the new dma_request_chan() the client driver does not need to look for
the DMA resource and it does not need to pass filter_fn anymore.
By switching to the new API the driver can now support deferred probing
against DMA.
Signed-off-by: Peter Ujfalusi <peter.ujfalusi@ti.com>
CC: Ulf Hansson <ulf.hansson@linaro.org>
CC: Jarkko Nikula <jarkko.nikula@bitmer.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
And return the old clock rate if something went wrong.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Tested-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
We had a regression on r8a7740 where the SDHI clock was a generic
peripheral clock, so changing its rate was not desired. This should be
fixed in the clock driver. However, it also shows that the new clock
calculation should only be used on tested systems. Add a check for that.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Tested-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
RCar Gen2 and later implementations of TMIO/SDHI have their own set of
features and additions. FAST_CLK_CHG is just one of them and I see a few
others being added soon. Some may work on older chipsets but this needs
to be tested case by case. Instead of adding a bunch of flags for each
feature, add a global RCar2+ one for now. We can still break out
features if the need arises.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Tested-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Save a few lines, the codebase is large enough.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Tested-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
With the new dma_request_chan() the client driver does not need to look for
the DMA resource and it does not need to pass filter_fn anymore.
By switching to the new API the driver can now support deferred probing
against DMA.
Signed-off-by: Peter Ujfalusi <peter.ujfalusi@ti.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The controller claims to support SDR104. In fact, it only supports a
degraded SDR104 since the maximum frequency of the SD clock is 120 MHz
instead of 208 MHz.
The sdhci core is unaware of it and will compute a wrong clock divider.
We can deal with this specific case by using presets.
Signed-off-by: Ludovic Desroches <ludovic.desroches@atmel.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Some boards need different pin drive strength for the UHS mode. Add an
optional pinctrl setting with two pin states covering UHS speeds and
other speeds.
Signed-off-by: Lars Persson <larper@axis.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Add a start_signal_voltage_switch() operation to support enabling of
UHS modes.
Signed-off-by: Lars Persson <larper@axis.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The driver in its current form does not support UHS at all due to
a missing start_signal_voltage_switch callback.
Also when this callback is added we should let the device tree control
UHS capabilities using the standard mmc bindings.
Signed-off-by: Lars Persson <larper@axis.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Now that reading CTL_STATUS is consistent, we can remove CTL_STATUS2 and
document how this is handled internally.
Reviewed-by: Simon Horman <horms+renesas@verge.net.au>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
This bit has a different meaning in SDHI and original TMIO. Document
that and use the proper naming.
Reviewed-by: Simon Horman <horms+renesas@verge.net.au>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
To prevent confusion, use the virtual u32 CTL_STATUS in card_busy() the
same way as in other parts of this driver.
Reviewed-by: Simon Horman <horms+renesas@verge.net.au>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
BIT() makes it easier to match the bits to the datasheet. This is
especially important here, since some variants have different names in
their datasheets (like with Renesas R-Car).
Reviewed-by: Simon Horman <horms+renesas@verge.net.au>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Looking at the backlogs, I am not the only one who missed that the above
functions do not read u32 from one register, but create a virtual u32
from reading to adjacent u16 registers (which depending on 'bus_shift'
can be up to 8 byte apart). Because this driver supports old hardware
for which we don't have documentation, I first wrongly assumed there was
a variant which had a few u32 registers. Let's give the functions more
descriptive names to make it more obvious what is happening.
Reviewed-by: Simon Horman <horms+renesas@verge.net.au>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The legacy user space for n900 relies on the MMC slot names.
Let's check if those are passed in pdata and use them.
As this makes the DT booting compatible with legacy booting,
we should be able to start dropping omap3 legacy booting
support in v4.8.
Cc: Ulf Hansson <ulf.hansson@linaro.org>
Cc: Kishon Vijay Abraham I <kishon@ti.com>
Cc: linux-mmc@vger.kernel.org
Signed-off-by: Tony Lindgren <tony@atomide.com>
Tested-by: Ivaylo Dimitrov <ivo.g.dimitrov.75@gmail.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
There is no support for this platform in the kernel anymore.
Reported-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Acked-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
There is no support for this platform in the kernel anymore. Make the
Kconfig text more generic, so it won't get stale anymore.
Reported-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Acked-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
A last minute fix applied by Ulf made room for some simplification.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Acked-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
There is no reason to have a public and private header file. Merge them
into a private one, so looking up symbols is less confusing.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Acked-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Having just one irq handler again, let's include the 'card_status'
function in the main handler which is way more readable. Drop a useless
debug output while here. It should be a dev_dbg in case we ever need it
again.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Acked-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
We removed installation of separate handlers previously, so we can also
remove the separate handlers.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Acked-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
There is no user left in the kernel, so this code can be removed.
(Legacy, non-DT sh_mobile boards have been removed a while ago.) The
diff looks more complicated than it is: The if-block for multiplexed isr
is now the main code path, the rest is removed.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Acked-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
We won't access an index based array to get our DT config, but create
separate structs instead. So, remove the array which only wastes memory.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Acked-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
defined(CONFIG_LEDS_CLASS) || (defined(CONFIG_LEDS_CLASS_MODULE) && \
defined(CONFIG_MMC_SDHCI_MODULE))
is equivalent to:
defined(CONFIG_LEDS_CLASS) || (defined(CONFIG_LEDS_CLASS_MODULE) && \
defined(MODULE))
and it can also be written shortly as:
IS_REACHABLE(CONFIG_LEDS_CLASS)
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
SDHCI_SDR104_NEEDS_TUNING was originally named SDHCI_HS200_NEEDS_TUNING
and was added in commit 069c9f1428 ("mmc: host: Adds support for eMMC
4.5 HS200 mode").
That commit conflated SDHCI_SDR50_NEEDS_TUNING and SDHCI_HS200_NEEDS_TUNING
due to what appears to be misplaced parentheses.
Commit 156e14b126 ("mmc: sdhci: fix caps2 for HS200") made HS200
configuration equivalent to SDR104 configuration, renaming
SDHCI_HS200_NEEDS_TUNING to SDHCI_SDR104_NEEDS_TUNING despite tuning for
HS200 now being non-optional.
The mix-up with SDHCI_SDR50_NEEDS_TUNING remained and became more obvious
after commit 4b6f37d3a3 ("mmc: sdhci: clean up sdhci_execute_tuning()
decision") where the author noted the patch was "reflecting what the
original code was doing, it shows that it may not be what the author
actually intended."
The way the code is currently written, SDHCI_SDR104_NEEDS_TUNING
causes tuning to be done always for SDR50 mode if SDR104 mode is
also supported by the host controller. That makes no sense because
we already have capabilities bit SDHCI_USE_SDR50_TUNING and
corresponding flag SDHCI_SDR50_NEEDS_TUNING for that purpose.
Given the dubious origins of SDHCI_SDR104_NEEDS_TUNING, it seems
reasonable to remove it. The benefit being SDR50 mode will now not
un-nessessarily do tuning.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Swap the call order of sdhci_alloc_host() and platform_get_irq().
It makes sdhci_alloc_host() the last function that can fail in the
sdhci_pltfm_init(). So, we can drop the sdhci_free_host() call from
the failure path.
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Call devm_ioremap_resource() right after platform_get_resource().
This saves the error check of platform_get_resource() because
devm_ioremap_resource() checks if the given resource is NULL.
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The chain of devm_request_mem_region() and devm_ioremap() can be
replaced with devm_ioremap_resource(). Also, we can drop the error
messages because devm_ioremap_resource() displays similar messages
on error.
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Use the managed variant of ioremap().
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Use the managed variant of request_mem_region().
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The function platform_get_irq() can fail; it returns a negative error
code on failure. A negative IRQ number will make sdhci_add_host() fail
to request IRQ anyway, but it makes sense to let it fail earlier here.
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The requirement resource_size >= 0x100 may not necessarily be
reasonable; for example, sdhci-dove appears to sidestep some
registers in sdhci_dove_readw().
Moreover, current code displays an error message for too small
resource size, but still moves forward.
Every DT should be responsible for describing its properties
correctly, so lets's remove this error message from the common
framework.
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
ifdef's make the code more complicated and harder to read.
Move all the LED code together to reduce the ifdef's to
one place.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Some error paths in sdhci_add_host() simply returned without
cleaning up. Also the return value from mmc_add_host()
was not being checked.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Set MMC_CAP_AGGRESSIVE_PM for Broxton host controllers.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Set MMC_CAP_AGGRESSIVE_PM for Broxton host controllers.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
SDHCI_QUIRK2_NEED_DELAY_AFTER_INT_CLK_RST quirk is not used anymore so
remove it.
Signed-off-by: Ludovic Desroches <ludovic.desroches@atmel.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Disabling the internal clock while configuring the SD card clock can
lead to internal clock stabilization issue and/or unexpected switch to
the base clock when using presets.
A quirk SDHCI_QUIRK2_NEED_DELAY_AFTER_INT_CLK_RST was introduced to fix
these bugs. The cause was assumed to be a too long internal
re-synchronisation but it seems in some cases the delay (even if longer)
doesn't fix this bug. The safest workaround is to not disable/enable the
internal clock during the SD card clock configuration.
Signed-off-by: Ludovic Desroches <ludovic.desroches@atmel.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
In order to remove the SDHCI_QUIRK2_NEED_DELAY_AFTER_INT_CLK_RST and to
reduce code duplication, put the code relative to the SD clock
configuration in a function which can be used by hosts for the
implementation of the ->set_clock() callback.
Signed-off-by: Ludovic Desroches <ludovic.desroches@atmel.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
There are no need to have two versions of sdhci_runtime_pm_bus_off|on(),
depending on whether CONFIG_PM is set or unset. Thus it's easy to move the
implementation of these functions a bit earlier to avoid the unnecessary
pre-definition of them, so let's do that.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
A platform_driver does not need to set an owner, it will be populated
by the driver core.
Signed-off-by: Masahiro Yamada <yamada.masahiro@socionext.com>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Commit 9250aea76b ("mmc: core: Enable runtime PM management of host
devices"), made some calls to the runtime PM API from the driver
redundant. Especially those which deals with runtime PM reference
counting, so let's remove them.
Moreover as SDHCI have its own wrapper functions for runtime PM these
becomes superfluous, so let's remove them as well.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Adrian Hunter <adrian.hunter@intel.com>
Commit 9250aea76b ("mmc: core: Enable runtime PM management of host
devices"), made some calls to the runtime PM API from the driver
redundant. Especially those which deals with runtime PM reference
counting, so let's remove them.
Cc: Ian Molton <ian@mnementh.co.uk>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Commit 9250aea76b ("mmc: core: Enable runtime PM management of host
devices"), made some calls to the runtime PM API from the driver
redundant. Especially those which deals with runtime PM reference
counting, so let's remove them.
Cc: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Commit 9250aea76b ("mmc: core: Enable runtime PM management of host
devices"), made some calls to the runtime PM API from the driver
redundant. Especially those which deals with runtime PM reference
counting, so let's remove them.
Cc: Adrian Hunter <adrian.hunter@intel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Commit 9250aea76b ("mmc: core: Enable runtime PM management of host
devices"), made some calls to the runtime PM API from the driver
redundant. Especially those which deals with runtime PM reference
counting, so let's remove them.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Commit 9250aea76b ("mmc: core: Enable runtime PM management of host
devices"), made some calls to the runtime PM API from the driver
redundant. Especially those which deals with runtime PM reference
counting, so let's remove them.
Cc: Chaotian Jing <chaotian.jing@mediatek.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Commit 9250aea76b ("mmc: core: Enable runtime PM management of host
devices"), made some calls to the runtime PM API from the driver
redundant. Especially those which deals with runtime PM reference
counting, so let's remove them.
Cc: Russell King <linux@arm.linux.org.uk>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Commit 9250aea76b ("mmc: core: Enable runtime PM management of host
devices"), made some calls to the runtime PM API from the driver
redundant. Especially those which deals with runtime PM reference
counting, so let's remove them.
Cc: Ludovic Desroches <ludovic.desroches@atmel.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Ludovic Desroches <ludovic.desroches@atmel.com>
Tested-by: Ludovic Desroches <ludovic.desroches@atmel.com>
When trying to use this driver with the common clock framework, enabling
the clock fails because it was not prepared. This fixes the problem by
calling clk_prepare and clk_enable in a single function. Ditto for
clk_disable_unprepare.
Signed-off-by: David Lechner <david@lechnology.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Unwiding from an error in davinci_mmcsd_probe was a mess. Some errors were
not handled and not all paths unwound correctly. Also using devm_ where
possible to simplify things.
Signed-off-by: David Lechner <david@lechnology.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Now, no dw_mmc variant drivers use this callback, let's
remove it.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
We combine what dw_mci_exynos_setup_clock does with init
hook to simplify the code
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
We remove setup_clock hook and combine it into
init hook to simplify the code
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Some of Exynos has the Security management Unit(SMU).
This patch adds the function for controlling SMU.
In future, if exynos needs to control SMU, it can be implemented
in "config_smu" function, not "init" function.
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
dmaengine_terminate_all is deprecated and should be
replaced by more explicit synchronous and asynchronous
terminate functions. This change is based on the
commit b36f09c3c4 ("dmaengine: Add transfer termination
synchronization support"). Currently dw_mci_stop_dma
may be called under the spinlock, let's migrate
dmaengine_terminate_all to async terminate. This could
avoid the race condition of use-after-free resouce of
dmaengine once slave-dma driver implement the synchronize
method.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Without MMC_CAP_ERASE support, we fail to mount partition
with "discard" option since mmc_queue_setup_discard is limited
for checking mmc_can_erase. Without doing mmc_queue_setup_discard,
blk_queue_discard fails to test QUEUE_FLAG_DISCARD flag, so we get
the following log from f2fs(actually similar to other file system):
mounting with "discard" option, but the device does not support discard
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
dw_mci_rockchip_pmops just copy-paste what dw_mci_pltfm_pmops
have done. Let's remove it.
Signed-off-by: Shawn Lin <shawn.lin@rock-chips.com>
Signed-off-by: Jaehoon Chung <jh80.chung@samsung.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Implement voltage switch, supporting modes up to SDR-50.
Based on work by Shinobu Uehara, Rob Taylor, William Towle and Ian Molton.
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Setting frequency to 0 is not enough, the clock explicitly has to be
disabled. Otherwise voltage switching (which needs SDCLK to be quiet)
fails for various cards.
Because we now do the 'new_clock == 0' check right at the beginning,
the indentation level of the rest of the code can be decreased a little.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Starting the clock is always done after frequency change anyhow, so we can
do it directly after the clock calculation and remove the specific calls.
This is the first part of doing proper clock de-/activation at calculation
time.
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Based on work by Shinobu Uehara and Ben Dooks. This adds the voltage
switch operation needed for all UHS-I modes, but not the tuning needed
for SDR-104 which will come later.
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Currently tmio_mmc assumes that the input clock frequency is fixed and
only its own clock divider can be changed. This is not true in the
case of sh_mobile_sdhi; we can use the clock API to change it.
In tmio_mmc:
- Delegate setting of f_min from tmio to the clk_enable operation (if
implemented), as it can be smaller than f_max / 512
- Add an optional clk_update operation called from tmio_mmc_set_clock()
that updates the input clock frequency
- Rename tmio_mmc_clk_update() to tmio_mmc_clk_enable(), to avoid
confusion with the clk_update operation
In sh_mobile_sdhi:
- Make the setting of f_max conditional; it should be set through the
max-frequency property in the device tree in future
- Set f_min based on the input clock's minimum frequency
- Implement the clk_update operation, selecting the best input clock
frequency for the bus frequency that's wanted
sh_mobile_sdhi_clk_update() is loosely based on Kuninori Morimoto's work
in sh_mmcif.
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Change the clk_enable operation to take a pointer to the struct
tmio_mmc_host and have it set f_max. For consistency, also change the
clk_disable operation to take a pointer to struct tmio_mmc_host.
Signed-off-by: Ben Hutchings <ben.hutchings@codethink.co.uk>
Signed-off-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
unnecessary indirection via 'struct device' back to omap_hsmmc_host
Signed-off-by: Andreas Fenkart <afenkart@gmail.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The string "MMCSDCLK" is not actually used for clock lookup, so can be
removed.
Signed-off-by: David Lechner <david@lechnology.com>
Acked-by: Sekhar Nori <nsekhar@ti.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
With the new dma_request_chan() the client driver does not need to look for
the DMA resource and it does not need to pass filter_fn anymore.
By switching to the new API the driver can now support deferred probing
against DMA.
Signed-off-by: Peter Ujfalusi <peter.ujfalusi@ti.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
As there are two callers of sh_mmcif_set_power() and because its only
additional action is to check for a valid regulator, let's just remove it.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Both from a runtime PM and clock management point of view, the ->set_ios()
code is unnecessary complex.
A suboptimal path is also executed when the mmc core requests a clock rate
of zero. As that happens during the card initialization phase, trying to
save power by decreasing the runtime PM usage count and gating the clock
via clk_disable_unprepare() is just superfluous.
Moreover, from a runtime PM point of view the core will anyway keep the
device active during the entire card initialization phase.
Restructure the code to rely on the ios->power_mode to understand when the
runtime PM usage count needs to be increased. Let's also deal with clock
rate changes by simply applying the rate.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
While accessing the device, make sure it stays active by increasing the
runtime PM usage count for it.
Let's also defer to enable runtime PM until we really need access to the
device. This also enables the error path in ->probe() to become simpler.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
eMMC HS-DDR no longer works on the A80, despite it working when support
for this developed.
Disable it for now.
Signed-off-by: Chen-Yu Tsai <wens@csie.org>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
The ignore_children flag is used only when CONFIG_PM is set, so let's move
it into that section within the struct dev_pm_info.
Move also the corresponding pm_suspend_ignore_children() API out of
device.h into pm_runtime.h, to be consistent with similar APIs.
Unfortunate this causes the Toshiba PCI SD mmc host driver to fail to
compile as it needs pm_runtime.h, so let's fix this here as well.
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Acked-by: Pavel Machek <pavel@ucw.cz>
Signed-off-by: Rafael J. Wysocki <rafael.j.wysocki@intel.com>
Baytrail eMMC/SD/SDIO host controllers have been known to
hang. A change to a hardware setting has been found to
reduce the occurrence of such hangs. This patch ensures
the correct setting.
This patch applies cleanly to v4.4+. It could go to
earlier kernels also, so I will send backports to the
stable list in due course.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Cc: stable@vger.kernel.org # v4.4+
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Tegra124 has been randomly hanging during system suspend when entering
the Tegra LP1 low power state. The hang is caused by the Tegra SDHCI
driver and linked to the UHS-I tuning sequence. Disabling the UHS-I
modes for Tegra124 prevents any hangs from occurring when entering
system suspend.
Unfortunately, the tuning sequence described in the public Tegra
documentation is incomplete and on inspection of the current tuning
sequence that has been implemented is also incomplete and may cause
problems. In the short-term it is safer to disable UHS-I modes for now
and fix later because it would be too large of a change to simply patch
now. Therefore, disable UHS-I modes for Tegra124.
Signed-off-by: Jon Hunter <jonathanh@nvidia.com>
Acked-by: Thierry Reding <treding@nvidia.com>
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
- sdhci: Fix regression setting power on Trats2 board
- sdhci-pci: Add support and PCI IDs for more Broxton host controllers
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Merge tag 'mmc-v4.6-rc1' of git://git.linaro.org/people/ulf.hansson/mmc
Pull MMC fixes from Ulf Hansson:
"Here are a couple of mmc fixes intended for v4.6 rc3:
MMC host:
- sdhci: Fix regression setting power on Trats2 board
- sdhci-pci: Add support and PCI IDs for more Broxton host controllers"
* tag 'mmc-v4.6-rc1' of git://git.linaro.org/people/ulf.hansson/mmc:
mmc: sdhci-pci: Add support and PCI IDs for more Broxton host controllers
mmc: sdhci: Fix regression setting power on Trats2 board
Add support and PCI IDs for more Broxton host controllers
Other BXT IDs were added in v4.4 so cc'ing stable. This patch
is dependent on commit 163cbe31e5 ("mmc: sdhci-pci: Fix card
detect race for Intel BXT/APL") but that is already in stable
since v4.4.4.
Signed-off-by: Adrian Hunter <adrian.hunter@intel.com>
Cc: stable@vger.kernel.org # v4.4+
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>